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| Well ID: 34-059-22579 | Loading map...
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| County: | |
| Municipality: | |
| Operator Name: | |
| Well Pad ID: | |
| Farm/Lease Name: | |
| First Permit Date: | |
| Last Permit Date: | |
| Spud Date: 1979-06-10 | |
| Unconventional: | |
| Horizontal: | |
| Producing: No | |
| Violations: 3 | |
| Latitude: 40.1640298199 | |
| Longitude: -81.4244892953 |
| PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
|---|
| PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
|---|
| INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
|---|---|---|---|---|---|---|
| -1569225142 | 2011-04-15 | No change in status of well it still remains idle, owner has not made any attempts to abate compliance notice. | ||||
| 1307568514 | 2011-06-08 | Well has been plugged resolving previous compliance notice issued 2/18/11. | ||||
| 170110392 | 2008-09-11 | PRODUCING WELL | ||||
| 202443992 | 2011-06-06 | On site to witness owner remove tubing and packer from well and then perforate casing@3975--85' with 10 shots and then they ran tubing back in well to set bottom hole and lime plug tomorrow. | ||||
| 246008288 | 2011-02-18 | Upon receiving complaint from landowner Dan Larrick of idle well on property met with him and inspected well site and found well to be idle and leaking gas around wellhead area there has been no production reported on well since 2002,all valves at wellhead were shut and there was no domestic hookup noted coming from well. Well is equipped with 8" surface casing and 4.5 production casing and 1.5" tubing and 2-100 bbl tanks and 1-65 bbl tank and separator in dike area.
Plug or Produce well or file for temporary inactive status, if well is placed back into production properly construct new dike around storage tanks. |
9-9-02 | |||
| 246008288 | 2011-02-18 | Upon receiving complaint from landowner Dan Larrick of idle well on property met with him and inspected well site and found well to be idle and leaking gas around wellhead area there has been no production reported on well since 2002,all valves at wellhead were shut and there was no domestic hookup noted coming from well. Well is equipped with 8" surface casing and 4.5 production casing and 1.5" tubing and 2-100 bbl tanks and 1-65 bbl tank and separator in dike area.
Plug or Produce well or file for temporary inactive status, if well is placed back into production properly construct new dike around storage tanks. |
NONE_ | |||
| 246008288 | 2011-02-18 | Upon receiving complaint from landowner Dan Larrick of idle well on property met with him and inspected well site and found well to be idle and leaking gas around wellhead area there has been no production reported on well since 2002,all valves at wellhead were shut and there was no domestic hookup noted coming from well. Well is equipped with 8" surface casing and 4.5 production casing and 1.5" tubing and 2-100 bbl tanks and 1-65 bbl tank and separator in dike area.
Plug or Produce well or file for temporary inactive status, if well is placed back into production properly construct new dike around storage tanks. |
NONE18 |