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34-013-20654

Well Details

Well ID: 34-013-20654
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2012-06-08
Unconventional:
Horizontal:
Producing:
Violations: 0
Latitude: 39.9761068032
Longitude: -80.8379987642

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1303550371 2012-12-17 On the day of my inspection completion efforts had not begun. There was no activity taking place. No violations noted.
-1333222979 2013-01-15 On the day of my inspection Ed Smith with XTO was on site. Basic was on site to drill out cement but they were waiting on pipe. No violations noted.
-1416092894 2012-10-19 Call from company man that rig had been fixed and they were back to drilling.
-1481130018 2012-10-25 On the day of my inspection the rig was drilling in the lateral section. No violations were noted.
-1503596207 2013-02-20 On the day of my inspection the Universal Well Services were stimulating the well. No violations noted.
-273165630 2012-10-05 Inspection revealed that they were at core point@10,120' rig was circulating well preparing to come out of hole to core potential producing formation.
-430586749 2013-05-16 On site with local inspector Andrew Corder to look over restoration work preformed at site and I told inspector Corder that once vegetation is fully established restoration work would be satisfactory.
-488702628 2014-02-27 On the day of my inspection the well had all equipment to be capable of production. No violations noted.
-887517782 2013-02-14 On the day of my inspection I was accompanied by Inspector Dave Ball. Universal Well Services was on site to stimulate the well. They had to wait on sand truck for a while. No violations noted.
109806723 2012-11-01 On the day of my inspection the rig was drilling in the lateral section at 13429ft. No violations were noted.
1342741658 2012-07-18 Inspection revealed that driller twisted off down hole motor and bit assembly and after several attempts to retrieve it decision was made to set plug in well bore and then directional drill around lost drill bit@6694' rig crew ran 6641' of drill pipe in well and set 600' plug with 520 sacks ,O-Tex was cement contractor cement plug top should be@600' will confirm when they go back in well to side track around lost down hole motor.
1350769989 2012-10-18 On the day of my inspection rig was still down and waiting on top head drive parts. No violations noted.
1867908711 2013-02-13 On the day of my inspection Universal Well Services was on site stimulating the well. I spoke with Ed Smith of XTO who advised that they will be completing 7 stages and drilling out the plugs after commencement of the stimulation. No violations noted.
2058010280 2013-01-31 On the day of my inspection the company was preparing for fracing operations. The earth pit was being filled with fresh water. Universal was present. No violations noted.
375593663 2012-11-07 On the day of my inspection rig was drilling the lateral section at 16,075 ft. TD will be 16,090ft. No violations noted.
475297944 2013-01-24 On the day of my inspection the shoe had been drilled out and perforations were made. Rig moving to 20653. No violations noted.