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34-121-23080

Well Details

Well ID: 34-121-23080
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2010-03-11
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.6012377207
Longitude: -81.5412392697

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1444184369 2010-01-04 A.D. not hooked up,well is equipped with 8" surface casing and 4.5' production casing and 1.5" tubing and 1-100 bbl tank.
-1681295675 2010-03-12 Stopped by service rig for update rig crew was rigging up to rip casing they ran tools in hole to 4750' and tried to get telegraph they parted pipe@4520' and started to pull casing, owner will open hole log well and then run tubing back into well to set required lime plug.
-32003725 2014-02-28 My inspection finds the well is equipped with tubing and rods. The well is produced by a pump jack. The tank battery consists of one 100 bbl tank, a separator and a meter. The identification is properly displayed and legible.
-844376196 2005-05-02 A.D. not being used,rabbit well 2-100 bbl tanks within dike area,will need dike work preformed when SPCC rules goes into effect.
1269123304 2010-03-19 On site to witness operator run 4.5" casing in hole and cement in place,they ran 2810' of 10.5# casing and Formation Cementing cemented it in place with 215 sacks Class A cement with 2% gel added,cement top should be @1650'.
2072401370 2010-03-10 Stopped at service rig for update on plug back operation, operator stated that tubing was hung in hole and they were going too run bare tools inside of tubing to check TD and perf tubing tomorrow and possibly set bottom hole plug if they are able to pump through tubing.
280981101 2004-03-15 Rabbit well,no violations noted on day of my inspection.
PL7647 Preliminary Restoration done information from Data Point