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Well ID: 34-155-21823 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1984-02-08 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 1 | |
Latitude: 41.2514449226 | |
Longitude: -80.5559969558 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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1393950633 | 2014-03-04 | I was on location to check compliance to Chief's Order 2014-43. My inspection found the well was equipped with a plunger lift unit. The valve leading to the flow line from the well was open. There was a domestic flow line coming off the 4.5" casing. The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank, and a heat, treated separator. The dike met containment requirements. The heat, treated separator has the proper spacing. The flow line valves leading to and exiting the separator were open. The lease road was in stable condition. Photos were taken of all the production equipment. The well was in production which was in non-compliance of Chief's order #2014-43. The well needs to be shut-in immediately. | NONE9 | |||
PL4073 | Preliminary Restoration done information from Data Point |