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Well ID: 34-155-23402 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1991-05-01 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 41.1568473975 | |
Longitude: -80.8596406482 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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1700757206 | 2014-05-08 | I was on location performing a status check inspection. I found during my inspection the well was in production. The well was a plunger lift unit. The tank battery consisted of a 100 barrel production tank and a separator. A dike surrounded the tank. An identification sign was properly posted on the separator. The production equipment spacing was in compliance. The lease road was in stable condition. The well was placed into production prior to House Bill 278. | ||||
357451119 | 2004-01-16 | Restoration approved . | ||||
821497260 | 2003-06-19 | Meets requirements for preliminary restoration. The tank battery consists of 1-100 bbl tank inside th dike and one separator outside the dike. |