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34-103-22565

Well Details

Well ID: 34-103-22565
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-05-15
Unconventional:
Horizontal:
Producing: No
Violations: 5
Latitude: 41.0535286781
Longitude: -81.7195678918

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1919395895 2013-05-15 This is a non-producing pump jack well. Brush and terees make entry into tank battery nearly impossible. Will contact producer to obtain production records and ascertain their intent. No other apparent problems noted at time of inspection.
1035144080 2009-04-13 Well valves are turned on and is in production. Fluid and gas is coming in to tank battery. Brush has been removed around tank battery. Identification is updated. NOV in compliance. Sun, 45 degrees.
1082730557 2004-04-23 Case # 04-011, Met with Tom Sours on site to discuss production reports . I advised him to update production reports with Erica Freeman by 5-7-2004. Well is in production. NONE9
1086792211 2004-06-09 Case # 04-011 in compliance.
45865963 2009-03-09 Requested by Nathan Vaughan to inspect well for his client Wilcare Corp. Gas chart was changed on 3-2-09. It is reading 100 psi natural gas flow. Pump jack is incapable of working due to belts on electric motor are broken. Well and tank battery needs maintenance. Heavy growth around tank battery needs removed. No identification on well or tank battery. 9-9-02
45865963 2009-03-09 Requested by Nathan Vaughan to inspect well for his client Wilcare Corp. Gas chart was changed on 3-2-09. It is reading 100 psi natural gas flow. Pump jack is incapable of working due to belts on electric motor are broken. Well and tank battery needs maintenance. Heavy growth around tank battery needs removed. No identification on well or tank battery. 9-9-05(A)10
584418787 2014-05-08 Inspected production well on 05/08/2014. The tank battery consists of 1-210 bbl steel tank, 1-100 bbl steel tank, and a production unit within an earthen dike. The diked area is located within a locked metal fence. Well identification is posted at the tank battery, but it lacks the operator name. The well is equipped with a pump jack with an electric motor located within a locked metal fence. Research into the production history of the well showed that it has not turned in production since 2010, therefore the well must be plugged. NONE
584418787 2014-05-08 Inspected production well on 05/08/2014. The tank battery consists of 1-210 bbl steel tank, 1-100 bbl steel tank, and a production unit within an earthen dike. The diked area is located within a locked metal fence. Well identification is posted at the tank battery, but it lacks the operator name. The well is equipped with a pump jack with an electric motor located within a locked metal fence. Research into the production history of the well showed that it has not turned in production since 2010, therefore the well must be plugged. NONEC
PL12144 Preliminary Restoration done information from Data Point