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34-121-24281

Well Details

Well ID: 34-121-24281
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2009-10-07
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.933320186
Longitude: -81.3281218775

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-14607847 2010-07-02 On site to witness first stage of frac job Producers Services preformed work,15 -500 bbls of fresh water was used on first stage with 50 gal of Pro Clay Firm LP,55 gal of Pro Slick,43 gal of Shale Slick, no sand was used on this job,perfs are as fpllows1594-1598(5) shots1660-1674(27)shots1808-1870(16) shots 1936-1972(14) shots 1998-2066(23) shots perforations were preformed by Timco Wire line Services.
-160624352 2012-05-07 Inspection of the well head found the following -4.5 production casing -1.5 tubing with the production valves open and the well being produced by the means of a pumping unit, A 100 barrel tank -1600 gallon plastic tank -separator and gas meter are present in an established dike with proper well identification.
1368706634 2013-05-16 I received a call from Sue Robertson at 11:59 am on 5-15-13. Mrs. Robertson stated that the well on her property had a small leak at the well head. I called Bill Woods with the Oxford Oil Co. and he said that he already had people in route to clean the spill. My inspection today finds the spill has been properly cleaned up and no oil was visible at the time of my inspection.
704361982 2011-01-10 Restoration work at site satisfactory, pit has been filled in and site restored and vegetation has been established.

Note: Well is equipped with pumping unit and tubing and rods and 2-100 bbl tanks with dike in place.