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34-069-20058

Well Details

Well ID: 34-069-20058
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1975-10-29
Unconventional:
Horizontal:
Producing: No
Violations: 3
Latitude: 41.3394149717
Longitude: -83.9571496311

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1220415853 2011-08-05 Well located in bean field. No lane to well. 4" casing with casing head, 2" tubing, and rods. No pumpjack on well. Well shut in on annulus and tubing. 72 psi still on guage on production lines. No guage on well. I.D. on site still identifies previous owner Aurora Energy. No production records since 2006. NONE_
1220415853 2011-08-05 Well located in bean field. No lane to well. 4" casing with casing head, 2" tubing, and rods. No pumpjack on well. Well shut in on annulus and tubing. 72 psi still on guage on production lines. No guage on well. I.D. on site still identifies previous owner Aurora Energy. No production records since 2006. NONE9
1220415853 2011-08-05 Well located in bean field. No lane to well. 4" casing with casing head, 2" tubing, and rods. No pumpjack on well. Well shut in on annulus and tubing. 72 psi still on guage on production lines. No guage on well. I.D. on site still identifies previous owner Aurora Energy. No production records since 2006. NONEC
1363115432 2013-01-31 At the time of the inspection the well was shut in and the gauge indicates 20 psi on the production line. There was no gauge on the annulus and no sign of any leaks. The corrective action from the Compliance Notice issued in 2011 has not been completed. The inspection was done at the request of Eric Vendel from The Ohio Division of Oil and Gas.
273667047 2012-01-04 No change from last inspection. NOV's from last inspection on 8/5/2011 still need resolved.