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34-121-62914

Well Details

Well ID: 34-121-62914
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1943-04-01
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.8522916885
Longitude: -81.3925934244

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1921627432 2013-08-19 I received a call from Jeff Miley stating that he would begin plugging on Joe Dimmerlings property. I called Mr. Dimmerling and informed him that plugging operations would be commencing on Tuesday.
-1961082696 2013-08-26 My inspection today finds Berry Well Service is attempting to retrieve 1" tubing and a packer from the well. The tubing parted at 135' and the rig is trying to get back a hold of the tubing with a spear. After a couple of attempt the rig crew was able to pull the tubing.
1367335392 2013-04-29 Inspection and complaint response per request of the landowner Joe Dimmerling. The landowner stated the well was idle and He was wanting to build a pond and encase the well within the boundaries of the pond. Inspector Eric Conrad and myself inspected the said well and Inspector Conrad will issue any violations needed. Our inspection found a idle well with no production flow lines hooked up. A complaint log was entered on 04/30/2013.
1377708463 2013-08-27 Appalachian ran a vdl bond log. The log showed a void from 590' up to 545'. Appalachian perforated the 2" tubing with three shots from 590' to 580'. The service rig ran tubing back to 1600'. Cemenco pumped a total of 34 sks of class A cement in five 300' stages. They then pumped on the 2" tubing and were able to push an additional 11 sks of cement. The cement stayed at surface. A valve was installed on the tubing to prevent the cement from moving.
1762427896 2013-05-03 On this day the landowner Joe Dimmerling called and was very much distraught to the fact that I had entered the property and issued a violation against the said well. I informed Mr.Dimmerling that this was actions taken due to His complaint on 04/22/13 He made to me stating the well was idle and He was going to bury it in a pond. Mr. Dimmerling demanded I stay off His property. I advised Mr.Dimmerling I had followed our standard operating procedures and policies according to the Ohio Revised Code 1509.