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Well ID: 34-111-24484 | Loading map...
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First Permit Date: | |
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Spud Date: 2014-06-19 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 39.8328640624 | |
Longitude: -81.3021826017 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1082138374 | 2014-07-16 | My inspection today finds the drilling rig, Patterson 342 is drilling a 8.75" hole at a depth of 9250'. | ||||
1403200153 | 2014-06-19 | The said well was spudded on this day by Express Energy with a proposed 100' of 32 conductor borehole to be drilled. | ||||
1479145555 | 2014-07-22 | Status check inspection on the drilling process found the current drilling depth to be 14,973' using a 8.5 directional drilling assembly with a current directional azmuth of 146.71 degrees and 3817 units of 3rd party gas present. | ||||
1514961832 | 2014-06-28 | I am onsite to witness surface cementing operations. Patterson rig 342 ran 349' of 18.635" casing. Allied Oil and Gas Services circulated 720 sacks of class A cement into place. I witnessed 65 barrels of cement return to surface. | ||||
443284723 | 2014-06-20 | The said well was spudded on 06/19/2014 by Express Energy's top hole rig with 100' of 32 conductor borehole being drilled and on 06/20/14 100' of 26 conductor was set and cemented to surface by Express Energy's cement services using 330 sacks of class A cement- 2% calcium-.50 pound per sack flow seal with 10 barrels of cement returns to surface. | ||||
803270917 | 2014-07-09 | Status check inspection found Patterson Drilling on the hole and the 12.250 diameter 2nd intermediate well bore has been drilled to a completed total depth of 7,147' and the company is pulling out of the hole with the drill string and preparing to run the 9.625 2nd intermediate casing string. | ||||
948612233 | 2014-07-02 | I am onsite to witness the first intermediate casing string cementing operations. Patterson rig 342 ran 2197' of 13.375" J-55 casing. Allied Oil and Gas Services cemented the casing in place with 394 barrels of class A cement. I witnessed good cement returns to surface. |