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34-059-24337

Well Details

Well ID: 34-059-24337
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-03-22
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.9782874965
Longitude: -81.4202493344

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-226322298 2014-06-23 On the day of my inspection, I witnessed Universal break circulation with fresh water then mix and displace five hundred forty two barrel of Type-1 cement to a depth of 315 foot, I witnessed 20 barrels of cement returns to surface with a weight of 15.6 and a yield of 1.20. My site inspection revealed no erosion and good vegetation, no spills to report and all fluid storage is setting inside containment.
1212700983 2014-03-25 On the day of my inspection I witnessed that Express Energy Services had drilled a 36 inch diameter hole to the depth of 115 feet and set 115 feet of 30 inch conductor pipe. Express Energy could not get conductor pipe plum. They are pulling pipe back out and will ream hole to 42 inches in diameter and rerun pipe and cement tomorrow.