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Well ID: 34-155-22833 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1986-01-22 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 41.1944952645 | |
Longitude: -80.9987163132 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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1017563449 | 2012-05-17 | My inspection of this well site found that the service rig tagged the cement top of the first plug at 2350 feet with wash over tools. | ||||
1286768796 | 2012-06-12 | My inspection of this well site found no violations. The service rig operator stopped milling at 2513 feet and was tripping out of the well. | ||||
1315646298 | 2012-05-30 | My inspection of this well site found the service rig shot-off the 1.5 inch tubing at 2400 feet. | ||||
1339520906 | 2012-05-09 | A bottom hole plug was pumped down the 4-1/2 inch casing. The 25 sack plug could not be displaced to the bottom of the well. The service rig was unable to pull the 1.5 inch tubing. Then a 40 sack cement plug was pumped through the tubing and displaced to the perforations. The plugging operation was postponed until an adequate amount of the obstructed casing can be removed from the borehole. | ||||
1339682535 | 2012-06-13 | I witnessed the completion of plug-back operations. The 4-1/2 inch production casing was ripped at 2371 feet. Tubing was ran down to 2675 feet on the outside of the 4-1/2 inch casing. A total of 110 sacks of cement was pumped in two stages and displaced to 2175 feet. | ||||
PL3538 | Preliminary Restoration done information from Data Point |