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34-153-22949

Well Details

Well ID: 34-153-22949
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2005-07-12
Unconventional:
Horizontal:
Producing: No
Violations: 6
Latitude: 41.0241002064
Longitude: -81.5762009226

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1336192475 2005-07-15 G&H Drilling is drilling on air in the top of the Big Lime. Should be near the salt later today. Will continue to monitor the site for any communication with Cargill.
-1675972990 2005-07-16 I received a call from George Dixon with G&H reporting that they encountered water flow at approximately 2617'. The flow was manageable but they would have to switch over to fluid. I called Cargill to see if they noticed a drop in the cavern pressure when flow began. I am waiting for their call back. Dilling will continue as long as the flow can be managed.
-2102999251 2006-05-05 The required fencing has been installed and the site has been graded. The charcoal filter, pressure relief valve and lightning arrestor still need to be installed. 9-9-02
-2102999251 2006-05-05 The required fencing has been installed and the site has been graded. The charcoal filter, pressure relief valve and lightning arrestor still need to be installed. 9-9-05(A)10
-709136511 2010-09-09 Status check inspection found no violations at this time.
-756561398 2005-07-08 HB 278 Inspection. Bailey Excavating is starting to clear and grade the location. G&H Drilling should be moving to the location on July 11.
-849402867 2005-07-11 HB 278 inspection - The drilling rig is moving on site and should start drilling with the next 24 hours. The first pit has been dug and will be lined for drilling the surface hole. The second pit will be dug tomorrow.
1120221408 2005-06-20 HB 278 pre-permit site inspection. After seeing the site, I contacted Columbus with recommendations for permit conditions.
1123267286 2005-07-25 G&H Drilling is moving off site. The drilling pits are full and need to be pumped down. I contacted Mike Schreiner who said that S&H would be on site later to at least take several loads.
151927778 2006-07-06 The violation has been corrected. 9-9-02
151927778 2006-07-06 The violation has been corrected. 9-9-05(A)10
1532275630 2006-04-04 Status check inspection found that the well was in production but the required fencing was not installed and the well identification had not been posted. Additional grading and seeding is also required before the preliminary restoration is approved. Restoration will be due by the end of April. 9-9-02
1532275630 2006-04-04 Status check inspection found that the well was in production but the required fencing was not installed and the well identification had not been posted. Additional grading and seeding is also required before the preliminary restoration is approved. Restoration will be due by the end of April. 9-9-05(A)10
1701286166 2005-07-14 G&H is drilling out from under surface casing. No violations at this time.
1809332372 2006-07-17 Preliminary restoration is approved.
319805247 2005-12-14 The site has been rough graded and the tank battery has been set. Preliminary restoration will be completed as the weather permits.
352378930 2008-07-29 I received a complaint from another landowner reporting a spill at the Bailey tank battery. It appears that one of the stock tanks was overfilled and a small amount of oil and/or brine was released into the tank battery. I will check again in 30 days to see what if any effect the spill had on nearby conifer trees.
532027009 2005-07-18 Fluid flow is being managed and G&H is drilling ahead at approximately five minutes per foot. The pit liner on the center divider has fallen and needs to be repaired.
708807139 2006-03-13 The well is in production. I contacted Mike Schreiner and told him that he needs to post the required ID, install the fencing around the well and the fencing around tank battery before the well goes into production. He said that he would contact Southway Fence to install the fencing and that he would post the required ID.