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Well ID: 34-059-24293 | Loading map...
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Spud Date: 2013-07-08 | |
Unconventional: | |
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Producing: No | |
Violations: 0 | |
Latitude: 39.9888535097 | |
Longitude: -81.3863819951 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-109862226 | 2014-01-28 | The site passed preliminary restoration according to 1509.072A. | ||||
-1275362273 | 2013-07-17 | On the day of my inspection, I witnessed the rig currently drilling for the 9.625" casing, there has been no spills to record, the location has containment control and erosion control. | ||||
-1561297818 | 2013-12-13 | On the day of my inspection, I found the well to be in production, Ergon was there loading oil from (1) of (8) four hundred barrel production tanks that is setting inside a steel sealed containment, there is (3) five hundred barrel fresh water tanks setting inside temporary containment on location, I placed a phone call to PDC Energy to inform them of proper I.D. needs to be posted at the entry and at the well. | ||||
1457029720 | 2013-06-25 | On this day of my inspection with Mike Hartshorn witnessed PDC Energy ran 100' of 30" conductor pipe. Express Energy Services cemented conductor back to surface with 64.41 bbls of class A cement with 2% calc. Displaced cement with 74.8 bbls of fresh water. Good returns of 10 bbls. |