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Well ID: 34-121-24433 | Loading map...
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Spud Date: 2013-08-04 | |
Unconventional: | |
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Producing: No | |
Violations: 0 | |
Latitude: 39.8839872508 | |
Longitude: -81.3930757615 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1225644165 | 2014-06-12 | My inspection today finds the well site meets the preliminary restoration requirements under 1509.072(A) of the Ohio Revised Code. The tank battery is comprised of eight 400 barrel tanks set in a liquid tight containment system. | ||||
1313647252 | 2013-08-07 | Express Energy Services on site with conductor rig they drilled to 100' with 32" bit and ran 100' of 26" casing and Allied Cementing pumped 336 sacks of Class A cement with a weight of 15.6 and a yield of 1.18 and they had 10 bbl of good cement returns to surface.
Note: Quantab reading taken on mix water indicated that it was fresh water. |
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857383631 | 2013-08-20 | My inspection today finds the drilling rig, Falcon rig 20, ran casing to 1993, Allied Well Service circulated 736 sks of class A cement into place. I witnessed 60 bbl of cement returns to surface. | ||||
92286805 | 2013-08-15 | My inspection today finds the operator has ran 18.625" casing to a depth of 376'. Allied cemented the casing in place with 736 sks of class A cement. |