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34-121-24433

Well Details

Well ID: 34-121-24433
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-08-04
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.8839872508
Longitude: -81.3930757615

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1225644165 2014-06-12 My inspection today finds the well site meets the preliminary restoration requirements under 1509.072(A) of the Ohio Revised Code. The tank battery is comprised of eight 400 barrel tanks set in a liquid tight containment system.
1313647252 2013-08-07 Express Energy Services on site with conductor rig they drilled to 100' with 32" bit and ran 100' of 26" casing and Allied Cementing pumped 336 sacks of Class A cement with a weight of 15.6 and a yield of 1.18 and they had 10 bbl of good cement returns to surface.

Note: Quantab reading taken on mix water indicated that it was fresh water.

857383631 2013-08-20 My inspection today finds the drilling rig, Falcon rig 20, ran casing to 1993, Allied Well Service circulated 736 sks of class A cement into place. I witnessed 60 bbl of cement returns to surface.
92286805 2013-08-15 My inspection today finds the operator has ran 18.625" casing to a depth of 376'. Allied cemented the casing in place with 736 sks of class A cement.