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34-059-24176

Well Details

Well ID: 34-059-24176
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2011-04-21
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.0575048578
Longitude: -81.6769364305

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1196040442 2011-04-07 Warren Drilling moving in on site, stopped and checked site for pit construction compliance and received update on possible conductor cement job.
-1207253645 2011-04-22 Stopped by drill rig for update they were spotting fluid tanks shale shaker and mud pump in preparation for down hole drilling program.
-1357178278 2011-05-18 Accompanied D. Ball on inspection. Well had been perfed that morning and to be acidized the next day. TD 7350.
-1826599568 2011-05-06 Stopped by drill site for update they were drilling on 9# mud@6574' should be logging hole later this evening.
-329267992 2011-05-27 Inspection revealed that well is equipped with 11" conductor pipe and 8.625 surface casing and 4.5" production casing and 2.375' tubing and 2-100 bbl tanks and separator within dike area.

Note: Horner Excavating was starting to reclaim site on the day of my inspection.

-70471574 2011-05-10 Inspection revealed that rig crew was tripping tools from well they twisted off@7230' and they got a hold of fish on first run and once removed from well they will replace broken drill pipe and then go back in well to drill to total depth.
-866902323 2011-05-18 Accompanied Dave Ball with Josh Garland on inspection. Tubing was being ran during visit.
1302559392 2011-04-11 Well spudded drilling conductor hole on fluid they except to run 200' of 11.75 conductor pipe, there is a water well approximately 250' due west of drill site.
1302910996 2011-04-15 On site to witness testing of BOP Assembly they tested blind ram@1000psi and we monitored pressure for 15 min with no decline then they attempted to test pipe rams and test failed they then proceeded to change out seal rings and retested and test failed again then decision was made to replace entire assembly will resume testing 4/18/11.

Note: Solidified mud pit and closed they are going to bring in steel tank to place cuttings in while drilling down hole.

1305244344 2011-05-12 Stopped by drill rig for update they were picking drill string back up to go in hole to remove bridge from well,they tried to log well and tools sat down@4160' operator stated they possibly would be ready to cement casing by tomorrow if all goes well.
1305419616 2011-05-14 Inspection revealed that rig crew ran 7340' of 4.5" casing in well and cemented it in place with 160 sacks 50/50 POZ and 150 sacks of Class A Rose Run blend cement plug down@7:50 a.m.
1305756840 2011-05-18 On site to witness bond log and perforating of casing top of cement@5700' and 36 shots @7225'-7275' owner will acidize well tomorrow.
1305928361 2011-05-19 On site to witness acid job Producers Services pumped 9800 gal of 15%acid and 1000 gal of 28% into perfs and displaced with H2O into formation and let soak for predetermined time and they started to swab it back into 300 bbl tank.
1307232792 2011-06-03 Restoration work continues at site.
1994983109 2011-04-27 Stopped by drill rig they were tripping bit@5172' should be back to drilling later today and they plan on coring Utica Shale section of well bore they have a 60' barrel on site and coring will be done on drilling fluid.
2031640025 2011-04-12 Stopped by drill rig for update on upcoming conductor job they were drilling on fluid@145' should be running and cementing pipe by late evening.
344733097 2011-04-25 Inspection revealed that rotary rig was drilling@3781' still dusting in lime TOL was noted@3496'.
363732111 2013-04-16 On the day of my inspection Reviewed the Divisions production records and found them to be current, there is 8.625" casing with 4.5" production casing and 2" tubing standing from the ground, all the valves are open at the well, there are (3) one hundred barrel production tanks/ compressor setting inside a containment dike, the separator is setting inside a containment dike, the I.D. is posted on the tanks.
491586832 2011-05-09 Stopped by drill rig for update on upcoming casing job they were drilling at 7115' on 9#fluid and Trenton top was noted@6417' with small gas show in top of formation.
514556378 2011-09-23 Inspection revealed that drill site has been restored and vegetation has been established.

Note: Will check site in spring too see if any remedial work needs to be preformed.

746135421 2011-05-11 Inspection revealed that drilling rig was drilling@7295' and proposed total depth will be 7350' they should be ready to run production casing in the morning.