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Well ID: 34-081-20535 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2012-08-22 | |
Unconventional: | |
Horizontal: | |
Producing: | |
Violations: 0 | |
Latitude: 40.2648301123 | |
Longitude: -80.6855420546 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-501777280 | 2013-10-11 | I was on location to pass preliminary restoration for this well. The frac has been completed and the drilling equipnment has been removed from the location. At this time preliminary restoration can be passed. | ||||
-540917936 | 2012-07-28 | I was on site to witness the cementing of the conductor casing. My inspection revealed that Precision Rathole has drilled a 32" hole to a depth of 45' and ran 30" conductor casing to a depth of 45'. O-TEX cemented the casing with 100 sacks. NOTE: This site is located in a reclaimed surface mine. Cement never circulated to surface; it stayed approximately 25' from surface. I advised Precision Rathole that they needed to get a ready-mix truck to top off the annular space between the 32" hole and the 30" casing. I advised them that they needed to complete the remedial cement job either tomorrow morning (Sunday) or Monday morning if they couldn't get a ready-mix truck on Sunday morning. | ||||
1280739123 | 2013-07-23 | I was on location to do a status check of this well. The well is shut in and currently has no production equipment on location. The well shows no annular pressures of any kind at this time. A new waste water drainage system has been installed on location and the erosion controls have been built up as well. There are no violations at this time. | ||||
1351713200 | 2012-10-31 | My inspection found that the lease road was well maintained with a locked gate. The well pad was fenced and contained one well with an assembled christmas tree wellhead onsite. The well contained a large amount of rainwater but it was contained on the pad and there was no water leaving the pad. A Whipstock crew was onsite pumping the rainwater off the pad over the barrier wall at a slow rate to reduce erosion. The well was surrounded by steel fencing and cement barriers. There are no violations at this time | ||||
1359652128 | 2013-01-31 | I was on location to inspect the Zimnox pad that was recently fracked the past week. The wellhead is currently surrounded by a cage and has concrete barriers around it. The location has a very large amount of water on it due to the rain and snow melt, a crew is currently on site pumping water off location. Some plastic containment was left on location and the strong winds have blow some against the fence in the corner. I have contacted Chesapeake to let them know that the fence is about to give way and to have someone pick up the containment so that it does not blow off location. | ||||
1362433839 | 2013-03-04 | I was on this location to check the status of the cleanup of the plastic containment that was blowing into fences and had the possibility of leaving the location. Currently there is a crew on site collectiong all left over containment. The blow containment has been removed and fixed. Onsite is also 3 frac tanks and a sand seperator for the processing of flowback from the hydrallic fracturing of this well. There are no violations at this time. | ||||
1363629649 | 2013-03-18 | I was informed that flairing on this location was occuring and would take 2 weeks to complete following the hydrallic fraturing of the well. The job and flairing has just been completed and the majority of the equipment removed from the site. Still on site is a Baker frac tank and the Weatherford flowback trailor. A new christmas tree wellhead has been assembled and the well is surrounded by steel fence and cement barriers. There are no violations at this time. | ||||
2012996225 | 2013-10-11 | I was on location to pass preliminary restoration for this well. The frac has been completed and the drilling equipnment has been removed from the location. At this time preliminary restoration can be passed. | ||||
350740173 | 2012-08-20 | I was on site to check the status of Nomac Drilling Rig # 311. My inspection revealed that Grant Smith Trucking is still moving the rig onto the site. My inspection also revealed that two cranes are being used to put the derrick onto the substructure. They advised me that they are hoping to get the derrick in the air today and spud the hole sometime before tomorrow morning. They are anticipating circulation problems while drilling below the 30" conductor casing, so they are going to have a 1000 barrels of polymer drilling mud and a 1000 barrels of water on site before drilling below the 30" conductor. My inspection revealed no violations at this time. |