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34-007-24408

Well Details

Well ID: 34-007-24408
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2006-06-16
Unconventional:
Horizontal:
Producing: No
Violations: 1
Latitude: 41.8503200165
Longitude: -80.9176800194

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1021939416 2006-08-02 Inspection showed company pumping fluid from blow pit into frac tanks .
-1138963771 2006-06-21 On site to test B.O.P. on surfsce casing . Test B.O.P. at 400 p.s.I. With no loss after 15 minutes .
-1151398993 2006-08-22 On site for solidification of drilling pits .
-157559799 2006-08-03 On site to collect soil samples in brine dumping area .
-1812257994 2006-06-15 Appalachian Drilling rigging up drilling rig . On site for lake plain pit constuction .
-2021875038 2006-06-22 On site to wittness flaring of gas . The first pocket of gas was encountered at 469' . Drilling at 1500' when I left site .
-402359752 2007-01-18 Remedial work has not been completed .
-465062785 2006-06-19 On site to test B.O.P. on coductor casing . Test B.O.P. at 250 p.s.I. With no loss after 15 minutes .
1154365724 2006-07-26 Arrived on site to find a 2 water pump set at n-w corner of blow pit . There was a 2 rubber hose from pump 40' then hooked to 2 plastic flowline . The 2 plastic line then run west on top of surface 600' when it turned north for another 300' . The line had a hammer union connection at this point , which was not connected . I then smelled a very strong odor of oilfield brine . There were sevaral large puddles of fluid running n-e of 2 plastic pipe . 1176 quantab readings of fluid showed chloride levels off the scale of the quantab { 6000+ ppm } . I then observerd a area of dead vegetation and trees in a 150' diameter along route brine traveled , the kill area the narrowed to 10'-20' and traveled another 250'+ n-e where the kill area ended . I then collected water samples at beginning of spill . I took several photos { water pump location , 2 plastic pipe & kill area } . Water samples were transported to lab for analsis . I contacted Bob Anderson and advised of immediate clean-up needed { remove all free standing brine from kill area } . The case # given to this investigation is # 06-013 in complaint log . 9-1-07
1904530516 2006-06-20 Driiling rig trying to kill gas to run surface casing .
1993919860 2006-09-29 There has been no soil removed per notice requirements .
351553476 2006-08-23 Pit solidification approved .
724360543 2006-08-09 Inspection showed no remedial has been done to remove contaminated soil .
989822243 2006-07-31 Inspection showed fluid in working pit had been lowered , blow pit was full to top . There has been no action to remove contaminated soil at this time .