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34-167-65914

Well Details

Well ID: 34-167-65914
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1939-11-26
Unconventional:
Horizontal:
Producing: No
Violations: 3
Latitude: 39.3913172072
Longitude: -81.3398890458

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-2069088125 2012-02-09 I talked with Brian Morris - he will have identification posted and annual production reported to Columbus in the next few days.
-2094152176 2014-08-19 Upon inspection, it was observed that no effort has been made to bring this well into compliance. The well has a "scissor jack" pumping unit tied into a shackle line system and a central power unit. Trees are down in several areas on top of the shackle lines, rendering the central power unit ineffective for pumping the well. I will contact Big M Petroleum and inquire about plans to plug and abandon the well.
-557080312 2012-02-07 My inspection this day due to complaint by landowner's son-in-law, Dave Eigel, that the wells are not commercial and he wants them plugged. Annual production was last reported in 2009 and 6 bbl was reported. The old well is equipped with a scissor pump jack and is being pumped by a central power unit. No identification was found. Old 70 bbl tank has very little dike, a 55 gal drum separator sitting on top of the tank with a water line into the creek. There is no indication the well is producing. The well needs plugged, put in production or TI filed for it and identification posted. 2/8/12 - Talked to Brian Morris and he will have identification up this weekend, production submitted for 2010 also. He says wells are above economic limits. 9-9-05(A)10
-557080312 2012-02-07 My inspection this day due to complaint by landowner's son-in-law, Dave Eigel, that the wells are not commercial and he wants them plugged. Annual production was last reported in 2009 and 6 bbl was reported. The old well is equipped with a scissor pump jack and is being pumped by a central power unit. No identification was found. Old 70 bbl tank has very little dike, a 55 gal drum separator sitting on top of the tank with a water line into the creek. There is no indication the well is producing. The well needs plugged, put in production or TI filed for it and identification posted. 2/8/12 - Talked to Brian Morris and he will have identification up this weekend, production submitted for 2010 also. He says wells are above economic limits. NONE_
-557080312 2012-02-07 My inspection this day due to complaint by landowner's son-in-law, Dave Eigel, that the wells are not commercial and he wants them plugged. Annual production was last reported in 2009 and 6 bbl was reported. The old well is equipped with a scissor pump jack and is being pumped by a central power unit. No identification was found. Old 70 bbl tank has very little dike, a 55 gal drum separator sitting on top of the tank with a water line into the creek. There is no indication the well is producing. The well needs plugged, put in production or TI filed for it and identification posted. 2/8/12 - Talked to Brian Morris and he will have identification up this weekend, production submitted for 2010 also. He says wells are above economic limits. NONEC
1910637675 2014-01-08 Well is equipped with a shackle line pumping unit. It is rusted due to inactivity. There is no identification on the well. The polish rod is shiny due to recent pumping. Off of the production tee, there is an elbow, a nipple, another elbow then black plastic line. It is broken several feet away from the well. A new pictures were taken. There were no production records submitted for the years 2010 or 2011. Records submitted for 2012 stated "0" production. I will contact well owner about this.
591281167 2008-05-22 Inspection this day found well with scissor jack, producing with central power. New tank has been set but no ID's yet - he said will get them up. Good dike.