X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-079-20206

Well Details

Well ID: 34-079-20206
Loading map...
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1983-08-19
Unconventional:
Horizontal:
Producing: No
Violations: 3
Latitude: 39.0129301079
Longitude: -82.634991556

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1966533562 2004-10-13 FOLLOW UP TO NOV # -822122755 Shut-in since early 2001; no one monitoring this well. Will contact company. NONE
-430201605 2012-11-08 Performed Temporary Inactive Audit for Artex's TI application. Dean Price, Artex's well tender for this well, accompanied me on this audit and provided access to this well. Checked all valves to be sure they were closed; no leaks were measured with the Honeywell PhD6 gas meter nor observed by myself; all gas lines on the sales side of the well head including the gas line to Jackson were empty according to Dean Harris and have been since this well was shut in. The well meets the requirements for TI status.
-822122755 2004-10-13 Shut-in since early 2001; no one monitoring this well. Will contact company. NONE
1348492469 2012-09-18 Inspected the three shut-in ARTEX wells (Trepanier 1&2, API 34079201020000 & API 34079201380000) and Garrett #2 (API 3407920206) with Don Huck (Exploration Manager for Artex) and Dean Harris (oiler for Artex). Found all three wells were leaking gas between the 2-3/8 inch production tubing and the $-1/2 inch intermediate csg at the tubing ring on the casing head. I expect them to contact me by this coming Thursday 09/20/2012 on what they plan to do or that they have corrected the problem. Don contacted me on Wednesday 09/19/2012 that the leak has been fixed. I field checked the wells with the Honeywell PHD6/PID gas meter and doused with bottle water covering where the leaks occurred, and there was no reading on the meter and no bubbles where the leaks occurred earlier. NONE18
1907278796 2004-10-13 Extension of NOV deadline while company seeks new ownership of wells
1928613132 2007-08-02 Well has good id. Well is in production. Wellhead looks good. No violations at this time.
PL14883 Preliminary Restoration done information from Data Point