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Well ID: 34-079-20206 | Loading map...
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First Permit Date: | |
Last Permit Date: | |
Spud Date: 1983-08-19 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 3 | |
Latitude: 39.0129301079 | |
Longitude: -82.634991556 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-1966533562 | 2004-10-13 | FOLLOW UP TO NOV # -822122755 Shut-in since early 2001; no one monitoring this well. Will contact company. | NONE | |||
-430201605 | 2012-11-08 | Performed Temporary Inactive Audit for Artex's TI application. Dean Price, Artex's well tender for this well, accompanied me on this audit and provided access to this well. Checked all valves to be sure they were closed; no leaks were measured with the Honeywell PhD6 gas meter nor observed by myself; all gas lines on the sales side of the well head including the gas line to Jackson were empty according to Dean Harris and have been since this well was shut in. The well meets the requirements for TI status. | ||||
-822122755 | 2004-10-13 | Shut-in since early 2001; no one monitoring this well. Will contact company. | NONE | |||
1348492469 | 2012-09-18 | Inspected the three shut-in ARTEX wells (Trepanier 1&2, API 34079201020000 & API 34079201380000) and Garrett #2 (API 3407920206) with Don Huck (Exploration Manager for Artex) and Dean Harris (oiler for Artex). Found all three wells were leaking gas between the 2-3/8 inch production tubing and the $-1/2 inch intermediate csg at the tubing ring on the casing head. I expect them to contact me by this coming Thursday 09/20/2012 on what they plan to do or that they have corrected the problem. Don contacted me on Wednesday 09/19/2012 that the leak has been fixed. I field checked the wells with the Honeywell PHD6/PID gas meter and doused with bottle water covering where the leaks occurred, and there was no reading on the meter and no bubbles where the leaks occurred earlier. | NONE18 | |||
1907278796 | 2004-10-13 | Extension of NOV deadline while company seeks new ownership of wells | ||||
1928613132 | 2007-08-02 | Well has good id. Well is in production. Wellhead looks good. No violations at this time. | ||||
PL14883 | Preliminary Restoration done information from Data Point |