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34-009-22704

Well Details

Well ID: 34-009-22704
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-12-18
Unconventional:
Horizontal:
Producing: No
Violations: 20
Latitude: 39.2335591399
Longitude: -82.1384499015

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1025149170 2013-06-05 Met the company well supervisor and checked pressures on the injection tubing and annular space. No violations at well or pits. Year to date brine and truck totals reviewed.
-1058601064 2013-07-10 Dike is in good shape and unloading pad is good shape.
-1116558229 2012-01-05 Met with Dan Goins to review history of this well. Valve on injection was inoperable. Annulus had zero psi. functioning valves shall be put into place on injection tubing. Mini test will be performed in the near future to ensure Mechanical Integrity. 9-3-05(A)3
-1178382363 2006-04-21 Accompanied Joe Hoerst, who took a sample of the pit water.
-1202177929 2011-12-30 New needle valve had been installed on the annulus.
-1234106812 2003-03-17 No violations at this time.
-1258498324 2011-12-30 The injection side and annulus were tested while the pump was off and both registered 0 PSI. The pump was turned on and the injection side and annulus were tested again. Once again they both read 0 PSI. A company pressure gauge located at the pump read 350 psi so I believe there is a malfunction with my gauge.
-1297685562 2012-02-10 Follow-up on Compliance Notice, In-Compliance.
-1314071047 2012-03-21 Inspected well and storage area with Inspector Dan Goins. We discussed the unloading pad.
-1327803523 2012-11-14 Collected water sample from a BD Oil Gathering truck. UIC # 306. Water hauled from Ergon Water tank. Washington County Ohio. Lease # 0009. Accompanied by Morgan Button MRI2. Took samples to Jackson Office for shipment to ODNR Lab in Cambridge.
-1519823646 2009-03-12 The well was found without an ID.
-1565153251 2004-03-10 No violations at the time of inspection. Updated coordinates, which were off significantly.
-1614916539 2006-10-19 The pit was found full. Notified company. No action has been taken to comply with order.
-1647439260 2013-11-21 No violations at facility.
-1649199664 2006-10-23 Fluid level in the pit was approximately a foot below the top.
-168851628 2013-06-04 Unable to remove company gauge to check injection tubing pressure.
-1718896141 2012-11-15 Inspected injection facilities and checked injection pressure and annulus pressure. Collected a water sample from Weavertown Environmental Group (WEG) Truck UIC # 527. Water hauled from a 5000 gallon tank Permit 3 101532 Cecil, Pa. Took water sample to Cambridge lab.
-1827357313 2012-03-14 Accompanied Jon Scott on an injection well inspection. Noticed a couple of small areas of contaminated soils. We spoke to the well operator about remediation.
-1847380278 2006-12-15 No action has been taken to comply.
-1871237260 2006-04-04 Pit was found completely full. Called operator (4/4/06) and instructed him to take a load out of the pit ASAP. 9-3-04(A)
-1871237260 2006-04-04 Pit was found completely full. Called operator (4/4/06) and instructed him to take a load out of the pit ASAP. 9-3-07(G)
-1928223676 2012-06-13 Poured new concrete unloading pad. No notification was received on the construction of the pad. Pad has two drains that are connected to new 4" SDR 11 plastic line connected to concrete pit. A new 4" SDR 11 line was ran from the unloading pad to the concrete pit for unloading trucks. A 6" corrugated drain was ran for diversion of surface water around the up slope side of the new unloading pad. Well tender showed me a plastic jug attached to a stick and 2 gloves that were found floating in the pit. I suggested installing additional fencing around pit.
-1941781500 2013-05-21 Inspected injection pressure, annulus pressure, containment pit, and unloading pad. There were no trucks during inspection.
-1947677268 2012-02-10 Met with Dan Goins to check the pressures on the well.
-1975458245 2005-05-09 The fluid level was 4 inches from the top of the storage pit. The well needs tested. 9-3-07(G)
-1986797844 2014-01-27 Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Site was snow covered. Unloading pad was cleared of snow and ice.
-1989508424 2008-10-03 There were no violations found, at the time of inspection.
-1993940341 2012-03-22 Met Jon Scott at well to review records and reports and explain history on well to him before he takes over well for inspections.
-275312583 2013-05-09 Inspected injection tubing pressure, annulus pressure, containment pit, injection pump, and unloading pad. Injection operations are shut down by Carper Well Service to allow safe replacement of injection line fittings.
-276695570 2012-06-28 Water samples were taken from a Brine Tanker, BD Oil Gathering Corporation. UIC # 306. (Tanker had 143 barrels of produced water from Wilhelm Water tank Lease # 0004, Doddridge County West Virginia. Produced water was pulled from a 210 barrel tank.) Information taken from the Tanker log sheet. Took water samples from the concrete pit. Coordinated with ODNR Lab for pickup of samples in Marietta. Andy Thomas MRI 2 and Josh Garland MRI 2 assisted with the sampling.
-325960936 2001-05-31 FOLLOW UP TO NOV # 5609i205 An inspection revealed the 1/4" valve at the well on the injection side is in non working condition , the valve needs to be replaced. 9-3-05(A)3
-338182091 2004-08-17 No violations at this time.
-367176123 2013-04-09 Inspected containment pit, injection pressure and annulus pressure. Good identification on well. Updated GPS locations for well, lease road and containment pit (coordinates recorded in tank Lat and Long.)
-36830505 2006-08-14 No action has been taken to remedy violation.
-387670436 2010-11-17 Inspection this day found pump running, tubing has 20#, 0# on annulus. Water storage area/dike full but pump is running, should be lower. Good ID's.
-410095649 2002-03-07 FOLLOW UP TO NOV # 1269i854 An inspection of the well revealed some oily soil around a storage tank and below the storage impoudment, and a bare area below the well. NEED TO CLEAN UP ALL OILY SOIL AROUND TANK, AND STORAGE IMPOUNDMENT. SEED , MULCH, AND LIME BARE AREA BELOW WELL, ON 9-3-04(A)
-440310312 2012-01-05 Met Josh Garland at well site, checked injection and annulus pressures on well. 1/4 nipple needs replaced on injection side of well.
-496614638 2013-09-30 Inspected unloading pad, containment pit, injection pump, injection line, annulus pressure and injection pressure. There were no trucks on site during my inspection.
-564290163 2003-05-08 FOLLOW UP TO NOV # 2113127346 An inspection of the well site revealed a ditch cut across the lease rd., no way of entering and unloading brine for disposal. Well appears to be idle at this time. A M.I.T. test needs to be done on this well also. CALLED MR. CARPER ABOUT VIOLATIONS HE
-580104805 2008-06-17 Witnessed installation of the packer and tubing.
-590782139 2000-12-14 FOLLOW UP TO NOV # 1269i209 THIS WELL IS IDLE AND INCAPABLE OF INJECTING BRINE . THIS IS NO PRESSURE ON THE INJEC. OR ANNULUS OF WELL , WEEDS ARE GROWING UP IN THE STORAGE PIT AREA . POOR EQUIPMENT AT SITE , TALKED TO LEO ALTIER , HE SAID WELL WAS GOING TO SOLD AT THE SHERIFF'S OF 9-3-07(H)
-590782139 2000-12-14 FOLLOW UP TO NOV # 1269i209 THIS WELL IS IDLE AND INCAPABLE OF INJECTING BRINE . THIS IS NO PRESSURE ON THE INJEC. OR ANNULUS OF WELL , WEEDS ARE GROWING UP IN THE STORAGE PIT AREA . POOR EQUIPMENT AT SITE , TALKED TO LEO ALTIER , HE SAID WELL WAS GOING TO SOLD AT THE SHERIFF'S OF 9-3-07(J )
-599725272 2009-02-23 The pit was pumped down.
-644350372 2014-02-26 No noted violations.
-708413589 2013-11-21 Accompanied Inspector Josh Garland on this inspection. Site is in good order. Spoke with company man on site. No pollution or contamination observed.
-852014890 2002-01-22 FOLLOW UP TO NOV # 1269i707 An inspection of the well revealed that the pressure on the injection and annulus stillthe same, 85 lbs. Last inspection both sides where 40 lbs. Need a mini test done on this well. John Puterbaugh, also on site. 9-3-05 C
-852014890 2002-01-22 FOLLOW UP TO NOV # 1269i707 An inspection of the well revealed that the pressure on the injection and annulus stillthe same, 85 lbs. Last inspection both sides where 40 lbs. Need a mini test done on this well. John Puterbaugh, also on site. 9-3-07(G)
-88373296 2005-10-04 No action was taken to test the well.
-913076490 2003-09-18 No violations at the time of inspection.
-929186419 2012-01-25 Follow-up inspection revealed 1/4" valve has not been replaced on injection side and is still plugged off. Notified pumper of violation. 1/4" valve needs replaced. Water pump running at time of inspection, checked injection pressure at water pump. Josh Garland Athens County Inspector present at inspection. 9-3-05(B)4
-955454451 2012-04-02 Opened 4 1/2" annulus and released pressure. 2 7/8" annulus dropped at the same rate. Left 4 1/2" annulus valve open and pressured up the 2 7/8" annulus, both annulus spaces have communication. Put gauge on the 8 5/8" annulus gauge read 590 psi. Closed 4 1/2" annulus and tested to 310 psi for 15 minutes no loss. 1 1/2" injection tubing was pressurized with 500 psi. Contacted Tom Tomastik Underground Injection Control Geologist. Tom said to monitor the well at this time. There is no evidence of communication out side of the 4 1/2" casing.
-967967723 2007-09-10 No action has been taken to plug or operate the well.
-990366653 2008-02-27 Service rig was on the well.
1045144359 2003-02-06 No violations at this time.
1073326304 2003-07-16 No violations at the time of inspection.
1081069386 2013-04-17 Inspected unloading pad, containment pit, injection pump, injection pressure and annulus pressure. While on site a Carper Well Service truck arrived and unloaded brine from Grenadier leases Sizemore and Kuhn. Located in Wetzel County, West Virginia. I collected a brine sample from the Carper truck.
1081945350 2004-04-14 No violations at the time of inspection.
1083856599 2004-05-05 No violations at the time of inspection.
108858783 2008-06-27 The well failed a pressure test.
1089895241 2004-07-15 Fluid level, in the pit, approx. 1 1/2 feet below the top. Slight vacuum on tubing.
1090208574 2004-06-17 No violations at the time of inspection.
1106058474 2005-01-12 The pit appears to have been recently pumped down. The fluid level is 1.5 ft from the top.
1145218342 2006-04-05 The fluid level was about a foot below the top of the pit.

The well needs a MIT. Suspension order was issued 4/18/06.

1184529678 2007-07-13 No action has been taken since last inspection.
1184535131 2007-06-12 No action has been taken since last inspection. Accompanied by Joe Hoerst.
1184898863 2007-04-12 There were no violations at the time of inspection.
1232876203 2013-03-21 Inspected injection pressure and annulus pressure at wellhead. Inspected the unloading pad, containment pit, injection pump and grounds around the containment pit. Collected water sample from injection line between the filter and the injection pump. Water sample was taken to ODNR /DOGRM Lab in Cambridge.
1250 2002-07-30 Injection pressure on well, annulus side 10 lbs, injection side 20 lbs. There are some filters by pump that need to be hauled out and removed from site. Need to add some pressure on annulus side of well.
1251072283 2011-11-29 Company gauges had seized up and I was unable to remove them for the test. Company's gauges read 385 psi on annulus and 30 psi on injection. The power had just gone out there at the well and the operator was concerned with getting the power back online. I will return within a couple of days to perform the test again and have the operator remove the company gauges.
1269i1088 2002-06-03 Checked injection well, no violations.
1269i1413 2002-10-01 No violations.
1269i1524 2002-11-13 No violations at this time.
1269i209 2000-12-14 THIS WELL IS IDLE AND INCAPABLE OF INJECTING BRINE . THIS IS NO PRESSURE ON THE INJEC. OR ANNULUS OF WELL , WEEDS ARE GROWING UP IN THE STORAGE PIT AREA . POOR EQUIPMENT AT SITE , TALKED TO LEO ALTIER , HE SAID WELL WAS GOING TO SOLD AT THE SHERIFF'S OFFICE IN ATHENS CO. ON 12/13/2000 AT 10:00AM . 9-3-07(H)
1269i209 2000-12-14 THIS WELL IS IDLE AND INCAPABLE OF INJECTING BRINE . THIS IS NO PRESSURE ON THE INJEC. OR ANNULUS OF WELL , WEEDS ARE GROWING UP IN THE STORAGE PIT AREA . POOR EQUIPMENT AT SITE , TALKED TO LEO ALTIER , HE SAID WELL WAS GOING TO SOLD AT THE SHERIFF'S OFFICE IN ATHENS CO. ON 12/13/2000 AT 10:00AM . 9-3-07(J )
1269i707 2002-01-22 An inspection of the well revealed that the pressure on the injection and annulus stillthe same, 85 lbs. Last inspection both sides where 40 lbs. Need a mini test done on this well. John Puterbaugh, also on site. 9-3-05 C
1269i707 2002-01-22 An inspection of the well revealed that the pressure on the injection and annulus stillthe same, 85 lbs. Last inspection both sides where 40 lbs. Need a mini test done on this well. John Puterbaugh, also on site. 9-3-07(G)
1269i854 2002-03-07 An inspection of the well revealed some oily soil around a storage tank and below the storage impoudment, and a bare area below the well. NEED TO CLEAN UP ALL OILY SOIL AROUND TANK, AND STORAGE IMPOUNDMENT. SEED , MULCH, AND LIME BARE AREA BELOW WELL, ON WELL SITE. 9-3-04(A)
1269i984 2002-04-22 Follow-up on NOV, In-Compliance.
1280422291 2012-03-20 Meet with Dylan Harlow. 4 1/2 inch annulus and the 2 7/8 inch annulus have communication. Both have 250 psi on them. A small brine seep was located down slope from the unloading pad. In an effort to determine the source of the brine green dye was mixed with fresh water and poured down the unloading pad drain. No dye was observed at the seep location.
1281370976 2012-02-15 Checked unloading pad and storage area with Manager Rocky King, may need gravel and water breaks on lease road in spring.
1340897308 2012-06-28 Accompanied Jon Scott and Andy Thomas on water sampling inspection. Water samples were taken from the storage pits as well as UIC brine truck #306 which happened to be off loading at the time. Injection pressures and annular pressures were also tested at
1348093088 2012-09-19 Inspected site at request of Chief Simmers and inspection revealed that well was in operation and B&D Oil Gathering had tanker truck on unloading pad during inspection it was noted that unloading pad had been recently replaced and new lines going to containment pit has been replaced recently and area around facility has been mowed and area was clear of trash and other debris and several photo's were taken of site and will be placed into well file.
1348146093 2012-09-19 Inspected by request of Robert Worstall. Accompanied Dave Ball on inspection of the facilities and the well. The flow meter was not functioning at the time of inspection, but the operator was able to provide records that showed a total of 91,936 barrels had been received this year. B & D was unloading at the time of the inspection.
1348241852 2012-09-21 The line from the pump to the well had been replaced. The identification was corrected. The treatment for the soil was due to arrive early next week.
1351103313 2012-10-22 Salt water injection pump was in operation during inspection. Inspected the concrete pit, pump, injection line and unloading pad. No leaks were observed during inspection. The inline flow meter is broken. Brine hauling records were reviewed from the company ledger book.
1351337753 2013-02-06 Inspected injection pressure and annulus pressure. Inspected unloading pad and containment pit. Ground was snow covered and showed no signs of contamination. Witnessed Hunter Disposal Truck (UIC 387) unload brine while parked on the unloading pad. I collected a water sample from the truck. I transported the water sample to Jackson office. I sent the water sample to the Cambridge lab.
1354646818 2012-12-04 Accompanied Inspector Jon Scott on inspection. Reviewed annular and injection pressures. Because of the low pressure on the annular space between the injection tubing and the casing Jon Scott called for a Mechanical Integrity Test.
1354768478 2012-12-04 Inspected the surface facility and checked the injection pressure and the annulus pressure. Annulus pressure was zero. I called Dylan Harlow and told him that they need to test the annulus. Injection pumps were shut down until the test could be conducted. 9-3-07(F)
1362694336 2013-02-28 Inspected containment dike, unloading pad, injection pressure and annulus pressure. Accompanied by Kip Thompson MRI 2. Witnessed two BD Oil Gathering Trucks at the facility. The first truck (License number PVT 1149) was not labeled with their UIC number the truck was finished unloading when I arrived. The second truck (License number PVR 3634 ) was labeled with the UIC number UIC #306 (1.75" lettering) and Brine (3" lettering) although the lettering was not 4" in height. I called BD Oil Gathering and told the office staff that their trucks must be labeled correctly for all UIC brine hauling with-in the state. I also informed Dylan Harlow (Green Hunter) that they need to make sure that the trucks that are hauling to their facility are registered and labeled for brine hauling.
1371841170 2013-06-20 Inspected injection pressure, annulus pressure, containment dike, injection pump, injection line, unloading pad, and collected a brine sample from BD Oil Gathering truck UIC # 306. Brine sample was taken to lab.
1380197289 2013-09-23 Inspected the unloading pad, containment pit, injection line, annulus pressure, and injection pressure. Witnessed two BD Oil Gathering Trucks (UIC# 306) unloading brine. Both trucks had a completed brine log. The second truck license # PUV 7464 had the UIC # 306 label on the side of the tank. The label was 1.75 inches in height not 4 inches. There was no brine label on this truck. I gave the drive a copy of the brine hauler requirements. I collected a brine sample from the first truck. The brine sample was taken to the Jackson office for shipment to the ODNR Lab.
1387284532 2013-12-16 Inspected the unloading pad, containment pit, injection pump, injection line, annulus pressure, and injection pressure. Injection pump was not in operation during the inspection. There were zero brine trucks on site during the inspection. Site was snow covered. Good identification at the well and the building next to the unloading pad.
1393000133 2014-02-21 Inspected unloading pad, Containment pit, injection pump, injection line, injection pressure and annulus pressure. Good identification on the well and building. There were no brine trucks at the location during the inspection.
1398883768 2014-04-30 Inspected the injection pressure, annulus pressure, unloading pad, injection pump, containment pit and injection line. Collected brine sample from the injection line. Checked brine hauler records and truck UIC labeling.
1400266448 2014-05-16 Inspected the unloading pad, containment pit, injection line, injection pump, annulus pressure and injection pressure. Injection pump was off during inspection.
1401197926 2014-05-27 Pictures of site taken. Injection pressures tested at well while pump was running and while it was off. The injection pressure was 20psi while the pump was off and 380 while it was running, the annulus pressure was tested and found to be steady during both tests. No noted violations.
1405108231 2014-07-11 No noted violations.
1409183030 2014-08-27 Inspected the unloading pad, containment pit, injection pump, injection line, annulus pressure and injection pressure. Good identification posted on the wellhead and building near the unloading pad. Witnessed a Hall Drilling brine truck unloading on the pad. Reviewed the brine hauler records, Collected a brine sample and took the sample to the ODNR Lab.
156246569 2012-08-02 The gauge was too tight to remove, even with a back-up. When I attempted to remove the gauge from the 1/4" valve to check the annular space between the 2" tubing and the injection tubing I noticed it too was especially tight. In an attempt to apply enough pressure to remove the gauge I broke the 1/4" nipple at the point where it threads into the bull plug reducer. A 2" ball valve was closed behind the broken nipple so no pressurized fluids escaped the well. I called the company and they will be replacing the equipment tomorrow.
1582449554 2012-04-02 Witnessed Mechanical Integrity Test with Jon Scott.
1583919377 2012-01-25 Accompanied Dan Goins.
1607303759 2013-08-30 Inspected the unloading pad, containment pit, injection line, annulus pressure, and injection pressure. Identification at the wellhead.
1644883632 2013-01-22 Inspected the injection facility and checked the injection pressure and the annulus pressure. Injection pump is frozen. Green Hunter crew currently working to thaw out the pump.
1683640817 2012-10-01 Inspected injection pressure and annulus pressure. Inspected new injection line from the pump to the well. Inspected unloading pad while BD oil gathering tanker (UIC # 306) was unloading brine into containment pit. Reviewed hauling records for the well.
1687875146 2012-10-31 Collected brine sample from port on side of brine pump. Inspected unloading pad, concrete pit, injection pump, injection line and injection well. Checked annulus pressure and injection pressure at wellhead. Good identification at wellhead and unloading pad. Transported brine sample to Jackson office for shipment to Lab.
1687940961 2003-12-18 No violations at the time of inspection.
1688432579 2003-05-14 Follow-up on NOV, In-Compliance.
1705401668 2007-02-21 Frac tank was removed. A couple truck loads appear to have been taken from the pit. The well remains in noncompliance.
1736505040 2010-08-24 Inspection this day found pump not running, vacuum on tubing, 0# on annulus. Good ID's. Oil skim on water in dike area.
1782800456 2014-05-19 No noted violations.
1839027320 2010-03-09 Inspection this day found a nicer, cleaner facility than I am used to in Washington Co. - my 1st visit. Found pump not running, tubing on vacuum, 0# on annulus. Good ID's, said they are using the well small to moderate amount. Fluid about 1/5' down from top.
1935659109 2004-10-08 There were no violations at the time of inspection.
1953759868 2013-03-11 Inspected injection pressure and annulus pressure. Inspected the unloading pad, concrete pit, and injection pump. Reviewed the hauling log currently at 11,380 barrels.
1962343430 2014-01-13 Inspected unloading pad, Containment pit, injection pump, injection line, injection pressure and annulus pressure. Repairs have been made to the annulus. A 2" ball valve froze and busted on the annulus. The ball valve has been replaced. Accompanied by Andrew Adgate UIC Geologist.
2009924170 2012-12-05 Tested the annulus at 675 psi for 15 minutes. Initial test failed due to leak in the wellhead. Tightened the wellhead ring and tested again. Well annulus held 675 psi for 15 minutes with no loss. Smitty Vandall and Dylan Harlow were on site.
2050387968 2012-03-14 Jim Hubbard has been cleaning outside of dike North West corner. Excavated an area 2 feet by 1 foot and a second area 2 feet by 2.5 feet.
2061282767 2012-09-26 A vacuum truck was removing the skim of oil from the top of the fluids in the holding pit. Lime had also been applied to the soil in the area around the new flow line and load line as well as the well head.
2113127346 2003-05-08 An inspection of the well site revealed a ditch cut across the lease rd., no way of entering and unloading brine for disposal. Well appears to be idle at this time. A M.I.T. test needs to be done on this well also. CALLED MR. CARPER ABOUT VIOLATIONS HE SAID ATHENS COUNTY CUT THE DITCH ACROSS THE LEASE RD. TO STOP TRUCKS FROM ENTERING SITE. EXPLAINED TO HIM THAT THE WELL WAS IN VIOLATION AND A NOTICE OF VIOALTION WILL BE ISSUED TO PLUG OR PRODUCE WELL, AND A M.I.T. TEST NEEDS DONE. 9-3-07(G)
212813321 2009-02-18 The pit was found completely full. Notified operator via telephone.
2135370973 2008-01-16 The service rig was still on the well. No further action appears to have been taken to plug the well.
36892046 2013-02-27 Truck delivery at time of inspection. Carper well service, UIC-161. Good manifest, 125 bbl coming from CI McGowan Shattuck Pad 33.
38099222 2011-08-03 No violations at this time.
558786308 2014-07-03 Inspected the unloading pad, containment pit, injection pump, injection line, annulus pressure, and injection pressure. Identification is posted at the unloading pad and the well. Witnessed unloading of a Carper Well Brine Truck UIC # 25-161. Checked the brine hauler log sheet.
5609i205 2001-05-31 An inspection revealed the 1/4" valve at the well on the injection side is in non working condition , the valve needs to be replaced. 9-3-05(A)3
5609i245 2001-07-12 Folloe - up on N.O.V. , Non - Compliance , 1/4" valve has not been replaced or repaired on the injection side of the line at the well head. Also there is some oily soil that needs cleaned up below storage impoundment.
566599901 2006-07-14 No action has been taken to comply with the Chief's Order. The fluid level in the pit was approximately 1 1/2 feet from the top.
59773602 2012-06-28 Witnessed and assisted with the sampling of brine from the open pit.
652212545 2008-06-10 Rig and bulldozer were onsite. 1 1/2 inch tubing was on the trailer.
693552892 2005-09-16 Well needs tested.
706327766 2008-06-30 The well passed a pressure test.
716761238 2013-10-29 Inspected unloading pad, containment pit, injection pump, injection line, annulus pressure, and injection pressure. Identification is posted at the wellhead and the unloading pad.
761390138 2011-12-20 The pump was not running at the time of inspection. The injection pressure was 10 PSI. I was unable to inspect the pressure on annulus because 1/4" needle valve was corroded and unable to accept the gauge. I spoke with the pump house operator and asked to have valve replaced by 12/21/11. 9-3-05(A)3
787446481 2006-05-17 Conditions are the same. No evidence of recent activity.
843845335 2012-06-28 Josh Garland MRI 2 Inspected injection well injection tubing pressure and annulus pressure while water sampling was ongoing.
868535672 2006-04-27 Took water sample from frac tank. Prepared sample for shipment.
882152013 2008-12-03 There were no violations at the time of inspection.
914182433 2004-02-11 No violations at the time of inspection.
924835606 2003-04-22 No violations, county has dug a ditch across the lease rd., at this time there is no way of hauling brine into this site.
988178787 2008-09-30 No violations were found at the time of inspection.
iTOMK000134 2001-05-31
iTOMK000135 2001-05-31 1509.03 AND 1501:9-3-05(A)(3) - VALVE NEEDS REPLACED
UIC240 1987-06-03 1501:9-3-07(E)(F)
UIC325 1987-09-14 1501:9-3-07 (E)(F)
UIC330 1987-03-09 ACTION Legal 1501:9-3-07 (E)(F) Memo to Ralph M.