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34-029-21767

Well Details

Well ID: 34-029-21767
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-04-01
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.6841574884
Longitude: -80.8757222293

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1659405670 2013-03-13 I was at the site to check the progress on the conductor drilling operation. Express Drilling was on location and in the process of drilling the conductor hole for the Briceland Trust 8H. Once the 8H conductor hole was completed and casing installed, then the rig would move to the 5H and begin the conductor hole.
-2110591226 2013-03-26 I went to the site and had a pre-spud meeting with drilling consultant Derek Dupuis.
-539156511 2013-04-17
-919377905 2013-04-02
-957691495 2103-04-05
1363532675 2013-03-15 I was on location for the cementing of the conductor casing. The permit number and the emergency information were posted at the entry of the lease road. The pad was surrounded by a chain link fence with a main gate. The lease road was stable and drainage controls were in place. The topsoil had been piled at the south end of the pad. The soil was seeded and was covered in straw to prevent any soil from washing away. The permit for the well was posted inside the company trailer. Express Energy Services drilled a 26" diameter hole to 117'. Express installed 117' of 94lb, 20" OD casing. During drilling, the driller found that all the material was saturated with water and could not give me a precise depth as to where the water was coming from. O-Tex was the cementing contractor. Circulation was established. The cement was mudscaled at 15.6 pounds per gallon (ppg). O-Tex pumped 66 bbls of cement slurry at 15.6 ppg. The cement was displaced with 38 bbls of water. Cement returns to surface were observed. An estimated 25 bbls of cement returned to surface. Displacement was completed at 2:00pm.
296019430 2013-04-09
68499863 2012-12-11 I went to the site and conducted a pre-construction site inspection with Brett Bell, Chesapeake Field Representative.