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34-029-20702

Well Details

Well ID: 34-029-20702
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1973-10-12
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.8873447035
Longitude: -80.8996904817

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1576551266 2013-04-25 I was on location to the witness setting the last three plugs on the above well. After taking the wellhead apart there was no threads to screw a 4.5 collar and a pulling sub on to. Summit Well Service had to go to Baker Tools in Wooster Ohio to get a 4.5" "center spear". When they returned they pulled stretch and Appalachian shot the 4.5 at 3907'. Summit Well Svc. pulled 50.3' of 4.5" 11.6 # casing. Universal broke circulation pumped a 300' big lime cement plug 5455'/5755' displaced with 56 barrels of fresh water. Summit pulled 89 joints of 4.5 casing and Universal pumped 250' 8.625 plug 751'/1001'and displaced with 11.5 barrels of fresh water. Summit pulled 22 joints of 4.5 casing. Universal pumped a 250' surface plug. Job completed. I will follow up with final restoration report.
-400252070 2003-11-18 The tank battery consists of 3-100 bbl storage tanks, no salt water tank, no separator and no dike.
1370007974 2013-05-30 I performed a final restoration inspection on the above location. All stone was removed from the well location and stored in an area for the landowners use. The area was returned to a tillable field. Production equipment and flow lines and sales lines have been removed. FINAL RESTORATION IS PASSED.
2085113072 2013-04-25 I was on location to plug this well. Universal Well Service pumped fresh water ahead to kill the 600 psi. that was on the well. Started bull heading the bottom plug, the pressure started to increase. Universal slowed the rate to .8-.9 barrels a minute. They pumped 25 sacks of cement and displaced with 88 barrels of fresh water. Shut in over night.