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| Well ID: 34-059-24169 | Loading map...
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| County: | |
| Municipality: | |
| Operator Name: | |
| Well Pad ID: | |
| Farm/Lease Name: | |
| First Permit Date: | |
| Last Permit Date: | |
| Spud Date: 2010-08-11 | |
| Unconventional: | |
| Horizontal: | |
| Producing: No | |
| Violations: 0 | |
| Latitude: 40.0754619476 | |
| Longitude: -81.6538603824 |
| PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
|---|
| PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
|---|
| INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
|---|---|---|---|---|---|---|
| -1493630894 | 2011-01-06 | Restoration work at site satisfactory, pit has been filled in and site restored and vegetation has been established.
Note: Rabbit well equipped with 1-100 bbl tank with dike in place. |
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| -614606750 | 2010-08-24 | Stopped by drill rig to witness running of production casing, total depth of well was 7260' and operator is going to run 7249' of 10.5# casing in hole and cement in place with 150 sk of rose run blend cement. | ||||
| -818548779 | 2010-08-30 | Well owner preformed acid job on said well they placed 13,800 gal of acid into formation and displaced with fresh water back into formation, breakdown pressure was noted at 1650 psi and treating pressure was noted at 3200 psi and ISIP was noted at 710 psi and after five minutes it had declined to 683 psi,perfs are as follows7082-7181' with 95 shots recorded. | ||||
| 2072027287 | 2010-08-23 | Stopped by drill rig for update on drill in ,they were drilling@7165' and encountered flare stopped drilling and killed well then proceeded to drill on fluid to total depth. |