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34-153-20793

Well Details

Well ID: 34-153-20793
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-03-25
Unconventional:
Horizontal:
Producing: No
Violations: 12
Latitude: 41.0553647155
Longitude: -81.5951641725

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1254733903 2007-12-19 NONE
-1311993712 2004-03-18 The previous violation to plug or produce issued to Resource America is closed since the well has been sold to Murphy. The order will be issued to Murphy if efforts are not made to place this well back into production in the near future. NONE
-1809554036 2010-09-09 No change in the status or condition of this well and tank battery. The well is not in production nor has it been plugged and abandoned.
-315623915 2008-12-16 There has been no change in the status or the condition of this well. It is still idle and incapable of production.
-345827481 2008-05-05 No change in the condition or the status of this well which is idle and not capable of production.
-379146847 2006-11-15 No change in the operational status of this well. The flowline is still disconnected at the wellhead. NONE
1069385759 2007-05-03 Status check inspection to verify that the well was in production by May 2, as required by the consent agreement. The well was not in production nor was it capable of production on this day. The flowline was disconnected at the the wellhead and there was no chart on the meter in the tank battery. Photographs were taken showing the current condition of the surface equipment. NONE
1184094529 2007-04-25 Follow-up inspection with Supr. Cheslock. An Arvilla swab rig was on site working on the well. After the rig left, the well was not placed back in production. The deadline to plug or produce is May 2, 2007. NONE
1244925295 2003-12-12 Status check inspection - the last reported production from this well was 1995. According to Terry Whitehair with Resource America, no landowners are using gas from this well. The well must either be placed back into production or plugged and abandoned. NONE
1259885810 2009-01-21 There has been no change in the status of this well.
1313426978 2005-12-05 The well is idle and the CO has not been satisfied. NONE
1448103169 2007-04-10 No change in the status or condition of this well. The deadline to plug or produce is May 2, 2007. NONE
1559687051 2006-05-04 No change since the last inspection. The well is still idle and does not have the required identification. NONE
1651151335 2007-06-01 No change in the status of the well. The signed consent agreement required that the well be place back in production or properly plugged and abandoned by May 2, 2007. Neither requirement has been met. NONE
1904643198 2005-02-02 The well was transferred from Atlas America to Murphy Oil on February 26, 2004. The last reported production was 1995 and there is no domestic use. The well must be placed back into production or plugged and abandoned. NONE
356686719 2006-06-01 Follow up inspection with Supr. Cheslock on the Chief's Order to plug or produce. No change in the status of the well. NONE
387024796 2008-02-12 No change in the status of this well. The contempt hearing is still scheduled for 2/14 in Akron.
796307146 2013-04-27 I inspected this production property on 4/27/2013. The condition and status of this well and associated equipment has not been rectified since last ispected by Robert Worstall in 2011. The tank battery consists of a !00 Bbl. Stock tank, 25 Bbl. Brine tank, 2408 Gas separator with Gas measurement meter. Conversations with Brian Carr indicated that this well could possibly have a hole in the 4.5" casing, which would require a repair. The Flow line needs replaced according to Mr. Carr. Upon my inspection of the well head itself, I discovered a oil release that was around the 8.625 casing head. The size of the oil release 10' X 8' . The oil appeared to be oxidized and not recent. Pieces of the wellhead plumbing were missing and could be a source. This well has not reported production since 1995 and is incapable of production. No change since last inspection.
961146312 2005-02-02 FOLLOW UP TO NOV # 1904643198 The well was transferred from Atlas America to Murphy Oil on February 26, 2004. The last reported production was 1995 and there is no domestic use. The well must be placed back into production or plugged and abandoned.