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34-169-24685

Well Details

Well ID: 34-169-24685
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1990-09-08
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.9511634022
Longitude: -81.8085744049

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1355718939 2010-12-08 As part of the requirements for plugging and abandoning this solution mining well, Appalachian Well Surveys set a bridge plug in the 9-5/8" at 2298'. The bridge plug will be pressure tested as soon as arrangements can be made for a high pressure pump to load the hole. The well will then be plugged with cement from the bridge plug to surface.
-1799259591 2013-03-21 Appears to be in compliance.
-2088965351 2005-10-14 Test M.I.T. today and well passed
1067118771 2010-12-14 Whipstock Service rig is plugging well today with Universal Well cementing. Everything is frozen, pits ,trucks, me- water trucks
1131477281 2005-10-12 Arrive today for M.I.T and found that there was an equipment problem and test was cancelled .
1210i3457189 2002-03-27 Well appears ok. Brine drip leak noted at flange on line. Made this aware to Field Representative Mike Preattle. Accompanied by Tom T. & Dave H..
1346183544 2010-12-15 Tag plug at 1700 ft and run in with tubing and plug in stages to surface with Universal Well and Whipstock
1547966626 2005-10-14 M.I.T. for 8 hours and test passed.
16566 PASSED Y WITNESSED 6/25/91 INSPECTOR GREGORY, HAROLD DATE 06/2519/91 DATA FROM OLD VAX INFO
657419330 2010-12-10 As part of the required plugging process, an electric bridge plug was set inside of the 9-5/8" production casing at a depth of 2298' on 12/8. This depth is above the solution cavern and over 300' below the top of the Big Lime. On 12/10, the bridge plug was pressure tested to 500 psi and passed. J.Hawk Water Service provided the high pressure water pump to complete the test. The next step will involve placing cement inside the production casing and filling the casing to surface.
763395730 2003-12-09 CHECKED ID - OK