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34-009-23819

Well Details

Well ID: 34-009-23819
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2012-07-09
Unconventional:
Horizontal:
Producing: No
Violations: 1
Latitude: 39.2883214073
Longitude: -81.9106096507

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1070148011 2012-07-05 The pit is being constructed and the conductor will be set tomorrow morning.
-1273037103 2012-09-27 The pits have been closed. The pumping unit has been set and two 210 Barrel tanks are on site colleting flow-back water.
-1638573758 2012-07-10 Received call from R. Wolfe letting me know rig encountered large show of gas in the first Berea. Finished drilling 8 7/8" hole for intermediate string to 1600 feet. Formation Cementing was brought on site to pump gel to stabilize well. 48 sacks of gel were pumped at a rate of 4 Barrels per minute. Rate was insufficient and Superior Well service was called.
-1768686907 2012-07-12 Witnessed Blow-out preventer (BOP) test. After several attempts, the BOP held 500 psi. for 15 minutes.
-2005319615 2012-07-11 1574 feet of new 7" and 17lb/ft intermediate casing set in 1600 feet of 8 7/8 " wellbore with 250 sacks of class A cement. 600 lb Bentonite gel, 600 lb CaCl, and 70 lb celloflake used as additives. Cement was circulated to the surface and stayed at the surface. The lift pressure was 500 pounds.
-281072019 2012-07-16 Total Depth reached at 6200 feet. Well will be logged this evening and the longstring will be run tomorrow. Gas had created a micro annulus around the intermediate casing. I spoke with the company about installation of a well head to control the gas.
-50550464 2012-07-11 A mixture of 50 sacks Salt gel, 25 sacks of 50 lb starch, and 160 sacks of Barite were mixed with 120 Barrels of water and pumped down the well at 8 Barrels per minute to successfully stabilize the well.
-975708628 2012-07-24 I had spoken to Randy Wolfe about placing a pressure gauge and a pop-off valve on the surface-intermediate annular space on 7/19/12. The well did not have this equipment on it as of the time of inspection.
1155791366 2012-07-10 Currently drilling at 12227 feet. Plan to set intermediate string this evening.
1192195969 2013-03-01 Follow up to 1237419020. Casing still on site. Dike not done yet. Gauge on surface and intermediate casing reads 0 psi.
1237419020 2013-02-01 The pits have been closed and there is adequate vegetative cover. There is a small pile of casing on site including 4 1/2" production casing, conductor, rods, and 2" tubing. Failure to remove drilling equipment with in two months after completion. All equipment used in drilling shall be removed from the site. NONE5
1340226600 2012-06-20 Pre-site review with R. Wolfe.
1341589896 2012-07-06 Twenty five feet of 13 3/8" conductor set in 17" borehole today. Bedrock encountered at 15-20 feet.
1341839054 2012-07-09 60' of blow line staked out. Pit lined and fenced. Entry gated and signed. Currently drilling at 85'.
1341933080 2012-07-09 500 feet of 26 lb/ft 9 5/8 inch steel casing set in 540 feet of 12 1/4 inch borehole with 190 sack class A cement. Circulation established and good returns stayed at the surface.
1343228425 2012-07-25 No pop-off or gauge on valve. I spoke with R. Wolfe and he let me know he'd be putting a gauge on the surface casing head later this week.
1343413013 2012-07-27 No gauge or pop-off yet.
1343766936 2012-07-31 Filling pit today.
1344872283 2012-08-13 A gauge has been placed on the annular space between the surface casing and the intermediate casing. It read zero psi.
1347462396 2012-09-12 Witnessed frac job. 50,000 gallons used to treat well in the Medina formation. Perforations from 4747'-4757'. Formation break at 2286 psi, Instantaneous Shut-In Pressure 478 psi, 5-minute Shut-In 450 psi.
1355861731 2012-12-18 The pits have bee filled and there is adequate vegetative cover on site. There is still some drilling equipment on site. The dike is not finished yet.
1363702847 2013-03-19 Follow up to 1237419020. The casing has been removed.
162659483 2012-07-11 Superior well service was brought onto site to stabilize well. Two attempts were made to pump a gel mixture of 120 Barrels of water and 110 sacks of gel down the hole at a rate of 8 Barrels per minute. Neither attempt was successful so a barite additive will be brought in to thicken the gel.
314411928 2012-06-28 Checking stake distance to road.