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34-167-27796

Well Details

Well ID: 34-167-27796
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1984-10-16
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 39.549126814
Longitude: -81.4263662607

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-2134182691 2013-09-11 The lease road and the location have been graded and vegetation has been established on all areas. No production equipment was left on site. There is no trash on site. There is a piece of 2" flowline above the ground that was specified by the landowner to stay. Final restoration passed.
-639717858 2013-03-13 Witnessed the bottom hole plug being set. It was pumped through tubing.
-698151545 2013-03-22 Witnessed the bottom of surface casing, and the surface plug being set. Good circulation was achieved for both plugs. Accompanied by Inspector Jake Glascock.
1363713020 2013-03-19 I was on location to witness Alliance Drilling set the 100' rip plug. A cement bond log was run on the hole followed by a rip cut of the 7" casing at a depth of 856'. The plug was set using 30 sacks of regular class A cement and 30 barrels of displacement.
1364838037 2013-03-20 Witnessed several attempts to retrieve surface casing. No stretch was observed at the surface. Pipe was then backed off after it was tightened.