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34-111-22466

Well Details

Well ID: 34-111-22466
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2010-09-08
Unconventional:
Horizontal:
Producing: No
Violations: 1
Latitude: 39.8635309279
Longitude: -81.1341777979

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1082206381 2010-03-16 FOLLOW UP TO NOV # 681246172 FOLLOW UP TO NOV # 1271265617 Met with Land owner on complaint.RobinChristman and Ed Lucas. Well has not been making gas or oil. Well is supplied with a pump jack and 8 5/8 cas,4.5cas,2tubing.There is a 100 bbl and a 50 bbl.There has not been production since 2005.Well is capable. I called Mike Corp and will issue a written NOV.
-1340602766 2010-03-16 FOLLOW UP TO NOV # 66690924 FOLLOW UP TO NOV # 1270211762 Well is supplied with a pump jack and 8 5/8 casing ,4.5 casing,2tubing.Robin Christman called on the wells not producing.Well is capable.Called Mike Corp on the complaint.Company not filing production records since ownership.Gave Mike a verbal NOV.
-1616957831 2012-06-04 On the day of my inspection this site met the requirements of the ORC. Preliminary restoration is now passed.
-548591972 2013-10-29 Follow up review to complaint # 4517. On this day Inspector Eric Conrad and myself did a calculated approximation of the gas production and found the 2 wells involved in the complaint to be meeting the minimum standards of gas production. Our findings were as follows, The chart is a 30 day 100# chart on a 500# meter with a approximate line pressure of 3 psi =.75 mcf or 750 cubic feet of gas produced per day x 365 days in a calendar year = 273 mcf of produced gas per year meeting the State minimum of 100 mcf of gas per year per well.
-973305411 2010-03-16 FOLLOW UP TO NOV # 1270211762 Well is supplied with a pump jack and 8 5/8 casing ,4.5 casing,2tubing.Robin Christman called on the wells not producing.Well is capable.Called Mike Corp on the complaint.Company not filing production records since ownership.Gave Mike a verbal NOV.
1270211762 2010-03-16 Well is supplied with a pump jack and 8 5/8 casing ,4.5 casing,2tubing.Robin Christman called on the wells not producing.Well is capable.Called Mike Corp on the complaint.Company not filing production records since ownership.Gave Mike a verbal NOV.
1271265617 2010-03-16 Met with Land owner on complaint.RobinChristman and Ed Lucas. Well has not been making gas or oil. Well is supplied with a pump jack and 8 5/8 cas,4.5cas,2tubing.There is a 100 bbl and a 50 bbl.There has not been production since 2005.Well is capable. I called Mike Corp and will issue a written NOV. NONEC
1285813126 2010-09-29 On day of inspection Bill Arnholt w/Northwood Energy called and stated that they would be fracing well. At location we fracked the Berea and the Keener. The break down pressure on the Berea and the Keener was about 1200psi.Berea perfs were at 2034-2042.There were 17 holes. Keener perfs were at 1468-1478.There were 21 holes. We did not shut down between stages. We put first stage in and then 100 gal HCL before balls and 300gal of HCL after balls. We ran 25 balls on the ballout.Set pad and executed job. Ran 20%HCL on all job. Ran 20/40 sand and ran 30,000lbs.Stage 1 ran42,000gal of water. stage 2 ran 48,000gal water. Shut in pressure was at 1065psi.
1382993058 2013-10-28 Inspection per request of the landowner. Inspection of the well head found 4.5 production casing and 1.5 tubing with the production valves open and the well set up to be produced by the means of a pumping unit. A single 100 barrel production tank is present along with a mechanical separator and gas sales meter with a shared metering chart with the well identified as API # 34-111-22469-0000, I shall review the production reading of the chart at a later date, The landowner has asked that the old 100 barrel tank and 50 barrel tank along with the mechanical separator not in use and out of service be removed I will ask the company to remove these out of service items and properly remove unwanted vegetation around the site within 30 days along with posting proper identification.
1389104305 2014-01-07 Administrative inspection on this day to resolve the 3 prior unresolved compliance notices with the following API numbers- 66690924-1271265617 & 1270211762. The resolution of the violations was determined from a inspection I made on 10/29/2013 finding no violations present and the previous issues resolved.
66690924 2010-03-16 FOLLOW UP TO NOV # 1270211762 Well is supplied with a pump jack and 8 5/8 casing ,4.5 casing,2tubing.Robin Christman called on the wells not producing.Well is capable.Called Mike Corp on the complaint.Company not filing production records since ownership.Gave Mike a verbal NOV.
677657778 2010-03-16 FOLLOW UP TO NOV # 1271265617 Met with Land owner on complaint.RobinChristman and Ed Lucas. Well has not been making gas or oil. Well is supplied with a pump jack and 8 5/8 cas,4.5cas,2tubing.There is a 100 bbl and a 50 bbl.There has not been production since 2005.Well is capable. I called Mike Corp and will issue a written NOV.
681246172 2010-03-16 FOLLOW UP TO NOV # 1271265617 Met with Land owner on complaint.RobinChristman and Ed Lucas. Well has not been making gas or oil. Well is supplied with a pump jack and 8 5/8 cas,4.5cas,2tubing.There is a 100 bbl and a 50 bbl.There has not been production since 2005.Well is capable. I called Mike Corp and will issue a written NOV.