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34-121-23220

Well Details

Well ID: 34-121-23220
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2011-05-24
Unconventional:
Horizontal:
Producing: No
Violations: 4
Latitude: 39.7822043521
Longitude: -81.4726749895

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-2105148484 2011-06-03 On site to witness ripping of 4.5" casing Davis Well Service cut casing@4100' will pull Monday and log well and then run tested casing in well and cement it in place.
1124490222 2005-08-15 Upon inspecting well site found well to be idle all valves at wellhead are shut no production reported on well since 1993,well is equipped with tubing set at unknown depth 4.5 casing and is equipped with 1-100 bbl tank no visible I.D. could be found 9-9-05(A)10
1124490222 2005-08-15 Upon inspecting well site found well to be idle all valves at wellhead are shut no production reported on well since 1993,well is equipped with tubing set at unknown depth 4.5 casing and is equipped with 1-100 bbl tank no visible I.D. could be found NONE
1308780390 2011-06-22 On site to witness running of casing and cementing it in place rig crew ran a total of 4009' of used 4.5" casing in well and placed Dvtool@2706' and first stage cement volume was 190 sacks of cement and second stage was 200 sacks of classA cement
1311119175 2011-07-19 Fracking info 956 break pressure and treating pressure was noted@2204 and INSP was noted@1532 and 5 min pressure was 1289 and there was a total 316,222 bbl of water used and average pump rate was noted@44.8 bpm.
1332373705 2006-01-03 Well has been placed back into production resolving previous NOV. 9-9-05(A)10
1332373705 2006-01-03 Well has been placed back into production resolving previous NOV. NONE
1428042167 2009-10-06 Inspection revealed that well is on line and equipped with 8' surface casing and 4.5' production casing and 2.375" tubing possibly set on packer and there is 1-210 bbl tank located in dike area.
1531711584 2012-04-02 Inspection of well found 4.5 production casing -2.375 tubing with the proper production valves open and well being produced by means of a pumping unit, 210 barrel tank and separator with proper well identification found in an established dike.
776426569 2012-09-10 My inspection today finds the well is equipped with 4.5" casing, 2.375 tubing, rods, and a pump jack. The tank battery consists of one 210 bbl tank, a separator, and a meter inside of a dike with proper identification.
PL7550 Preliminary Restoration done information from Data Point