X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-067-21085

Well Details

Well ID: 34-067-21085
Loading map...
County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2012-08-26
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.4063181575
Longitude: -81.0346710746

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1329762510 2013-10-03 On the day of my inspection the site passed preliminary restoration according to 1509.072A. Made phone call to Matt Amos Drilling Foreman of Chesapeake Energy Corp and he referred me to John Snook Drilling Superintendent requesting that the cellars be pumped out on the Gotshall Pad and he confirmed that it would be done today.
-532932716 2012-08-27 Arrived on location for B.O.P.test 10:00pm till 3:30 am test approved.
1346849983 2012-08-27 Arrived on location for cementing of surface pipe , 13 3/8 pipe set at 615' with 530 sks of class a cement, covered job for mark moreland. He advised he wants to fill out all cement tickets when well is completed.
1353934782 2012-08-22 Set 100 ft of 20 inch conductor pipe and cemented with 265 sks - O-Tex Cementing Service. 26 inch hole. Set Tin Horn and cemented in place along with the conductor pipe. Had enough return on the cement to make a goog seal between Tin Horn and 20 inch casing.
1372141333 2013-07-29 Everything passed according to 1509.072A.