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37-021-21126

Well Details

Well ID: 37-021-21126
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County: Cambria
Municipality: Carrolltown Borough
Operator Name: AMER NATURAL RESOURCES LLC
Well Pad ID:
Farm/Lease Name: AMERICAN LEGION 1
First Permit Date: 2009-02-27
Last Permit Date: 2009-02-27
Spud Date: 2009-03-03
Unconventional: No
Horizontal: No
Well Status: ACTIVE
Violations: 0
Latitude: 40.609682
Longitude: -78.71038

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2010-0 31858.0 365.0 0.0 0.0 0.0 0.0
2011-0 26522.0 365.0 0.0 0.0 0.0 0.0
2012-0 5712.0 365.0 0.0 0.0 0.0 0.0
2013-0 9249.0 365.0 0.0 0.0 0.0 0.0
2014-0 3482.3 120.0 0.0 0.0 0.0 0.0

For data sources see[1]

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2010-0 PRODUCED FLUID 35.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273 FLUID RECOVERY SERVICE JOSEPHINE FACILITY JOSEPHINE PA
2011-0 PRODUCED FLUID 130.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273 FLUID RECOVERY SERVICE JOSEPHINE FACILITY JOSEPHINE PA
2012-0 PRODUCED FLUID 10.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273 FLUID RECOVERY SERVICE JOSEPHINE FACILITY JOSEPHINE PA

For data sources see[2]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1950486 2011-02-11 No Violations Noted Well Tag was present. At the time of inspection, no E&S issue. Well head consisted of 8﾿x 4﾿x 2﾿ production line. Production equipment of separator (50 psi), heater and data logger (50/25 psi) and 50 bbl brine tank (20 bbl fluid). No gas odor around well head and production equipment.
2034204 2012-01-13 No Violations Noted Well Tag was present. At the time of inspection, no E&S issues were present. Gas well was in production.


For data sources see[3]

References