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Well ID: 37-039-25233 | Loading map...
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County: Crawford | |
Municipality: South Shenango Township | |
Operator Name: D & L ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: BILES 2 | |
First Permit Date: 2007-09-18 | |
Last Permit Date: 2007-09-18 | |
Spud Date: 2008-03-05 | |
Unconventional: No | |
Horizontal: No | |
Well Status: ACTIVE | |
Violations: 0 | |
Latitude: 41.530379 | |
Longitude: -80.4176 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2008-0 | 1534.0 | 150.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-0 | 975.2 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-0 | 498.5 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2013-0 | 36.3 | 47.0 | 0.0 | 0.0 | 0.01 | 47.0 |
2014-0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2010-0 | PRODUCED FLUID | 132.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 34-007-22038 | PAROBEK #2 (SWIW #12) | OH | |
2011-0 | PRODUCED FLUID | 70.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | 34-099-23127 | NORTHSTAR #1 | YOUNGSTOWN | OH |
2012-0 | PRODUCED FLUID | 26.0 | Bbl | INJECTION DISPOSAL WELL | 34-007-20919 | RENSHAW / BRADNAN #1 (B&R) DISPOSAL WELL | PIERPOINT | OH |
2013-0 | PRODUCED FLUID | 24.0 | Bbl | INJECTION DISPOSAL WELL | 34-007-20919 | RENSHAW / BRADNAN #1 (B&R) DISPOSAL WELL | PIERPOINT | OH |
2014-0 | PRODUCED FLUID | 72.0 | Bbl | INJECTION DISPOSAL WELL | 34-007-24523 | MONROE #1 | WOOSTER | OH |
For data sources see[2]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
1690153 | 2008-03-07 | No Violations Noted | ||||
1690159 | 2008-03-06 | No Violations Noted | ||||
1690168 | 2008-03-05 | No Violations Noted | ||||
1829773 | 2009-09-22 | No Violations Noted | ||||
1963909 | 2011-04-05 | No Violations Noted | Upon inspection today I found this well shut-in, with the annulus buried and under water. The production equipment was comprised of a green steel stock tank , white poly tank and a heater/separator. All equipment was inside the diking. The production chart was inaccessible due to 18" of water covering the gravel inside. No violations. | |||
2125083 | 2012-12-20 | No Violations Noted | ||||
2203892 | 2013-09-12 | No Violations Noted | ||||
2341848 | 2015-02-06 | No Violations Noted |
For data sources see[3]