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Well ID: 37-063-29635 | Loading map...
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County: Indiana | |
Municipality: Rayne Township | |
Operator Name: XTO ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: A.E. BAKER FMLY E.C. BUCHHEIT 5 | |
First Permit Date: 1988-09-06 | |
Last Permit Date: 1988-09-06 | |
Spud Date: 1988-11-11 | |
Unconventional: No | |
Horizontal: No | |
Well Status: ACTIVE | |
Violations: 1 | |
Latitude: 40.736621 | |
Longitude: -79.125601 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1993-0 | 7358.0 | 106.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1996-0 | 7068.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1997-0 | 2789.0 | 46.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1998-0 | 147.0 | 2.0 | 0.0 | 0.0 | 0.0 | 0.0 |
1999-0 | 8798.0 | 153.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2000-0 | 8710.0 | 203.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2001-0 | 19117.0 | 367.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2002-0 | 13432.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2003-0 | 8094.0 | 229.0 | 0.0 | 0.0 | 0.0 | 229.0 |
2004-0 | 9206.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2005-0 | 8842.0 | 353.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2006-0 | 8338.0 | 357.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2007-0 | 6244.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2008-0 | 5711.0 | 351.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2009-0 | 4336.0 | 211.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-0 | 4529.0 | 351.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2011-0 | 4531.0 | 320.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2012-0 | 3145.0 | 366.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2013-0 | 2642.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2014-0 | 3709.0 | 365.0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2001-0 | BRINE | 390.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | ||||
2002-0 | BRINE | 51.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | ||||
2003-0 | BRINE | 0.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | ||||
2004-0 | BRINE | 70.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | ||||
2005-0 | BRINE | 80.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2006-0 | BRINE | 80.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2008-0 | BRINE | 100.0 | Bbl | BRINE OR INDUSTRIAL WASTE TREATMENT PLT | PA0101508 | PA BRINE | PA | |
2010-0 | PRODUCED FLUID | 55.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PAR000519462 | ADVANCED WASTE SERVICES OF PA LLC | NEW CASTLE | PA |
2010-0 | PRODUCED FLUID | 7.0 | Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026310 | CLEARFIELD MUNICIPAL SEWAGE TREATMENT PLANT | CLEARFIELD | PA |
2010-0 | PRODUCED FLUID | 7.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095443 | CREEKSIDE TREATMENT FACILITY | CREEKSIDE | PA |
2010-0 | PRODUCED FLUID | 1.0 | Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026034 | DORNICK PT SEWAGE TREATMENT PLANT | JOHNSTOWN | PA |
2010-0 | PRODUCED FLUID | 9.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2010-0 | PRODUCED FLUID | 1.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0020346 | PUNXSUTAWNEY BORO SEWAGE TREATMENT PLANT | PUNXSUTAWNEY | PA |
2010-0 | PRODUCED FLUID | 2.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 | TUNNELTON LIQUIDS TREATMENT FACILITY | SALTSBURG | PA |
2011-0 | PRODUCED FLUID | 70.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2012-0 | PRODUCED FLUID | 150.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2013-0 | PRODUCED FLUID | 116.0 | Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
2014-0 | PRODUCED FLUID | 119.0 | Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 | FLUID RECOVERY SERVICE JOSEPHINE FACILITY | JOSEPHINE | PA |
For data sources see[2]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
2166547 | 2013-05-06 | Violation(s) Noted | Admin inspt. Spill report received via e-mail on 5/6/13 at 1:46pm (See Attached).
Company rep Steve Smith reported to Department a 7.5 bbl brine release discovered at 1:00pm on 5/6/13. At this time, exact cause of release unknown, believed to be hole in production tank. Tank no longer leaking. No waterways reported to be affected. A follow-up inspection will be conducted in future to assess any environmental impacts of release and to ensure site is properly cleaned up and restored. Violations are being issued for this reportable release of production fluids under 25 PA CODE 78.54 in addition to 78.57, 91.34 and SWMA 301. |
667839 | 78.54 - Failure to properly control or dispose of industrial or residual waste to prevent pollution of the waters of the Commonwealth. | |
2169966 | 2013-05-22 | Outstanding Violations - No Viols Req'd | Response to spill incdt as follow-up to admin inspt record 2166547. Reported release of 7.5 bbl brine from fiberglass tank reported on 5/6/13.
Well-tender who discovered release on-site. WT suspects crack in tank as source of release largely due to groundhog burrowing under tank; believes burrow caused uneven support/pressure on bottom of tank, resulting in split. BT removed off-site. Impacted materials previously excavated, high composition of subsurface appears to be shale rock. Orange security fence surrounding area of excavation. Five roll-off boxes full of contaminated materials on-site. As per e-mail from XTO rep S. Smith, Opr is planning on following Act 2 and will submit a final report within 90 days. Dept recommends Opr installs new BT in secondary containment unit and/or utilize steel tank and continue to monitor and maintain well site throughout clean-up efforts as necessary. A follow-up inspection will be conducted to ensure that site is properly cleaned-up and restored. Outst viols exist, no new viols issued. |
|||
2217299 | 2013-10-29 | Outstanding Violations - No Viols Req'd | Follow-up in response to violations issued under inspection record 2166547 for the reportable release of production fluids on 5/6/13.
At time of inspection, well equipped for production. New brine tank installed, on gravel pad, appears sound. Well tag present, legible. Access road stable. Previously excavated area backfilled. Areas of disturbance seeded/mulched with no vegetative growth observed. Site temporarily stabilized. Department recommends Operator continue to monitor and maintain well site to ensure adequate vegetative growth is properly restored and temporary stabilization is maintained. Outstanding violations exist, no new violations noted at this time. |
|||
2235903 | 2014-01-13 | Outstanding Violations - No Viols Req'd | Follow-up in response to violations issued under inspection record 2166547 for the reportable release of production fluids on 5/6/13.
At time of inspection, well equipped for production. Well tag present, legible. Brine tank sound. Access road in good condition. Site temporarily stabilized with mulch, minimal vegetative growth observed. No accelerated erosion or sedimentation issues observed in relation to access road or well site at this time. Department recommends Operator continue to monitor and maintain well site to ensure adequate vegetative growth is properly restored and temporary stabilization is maintained. Outstanding violations exist, no new violations noted at this time. |
For data sources see[3]