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Well ID: 34-041-20160 | Loading map...
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County: Delaware | |
Municipality: | |
Operator Name: HARMAN PATRICIA A | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1964-10-20 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Active Injection | |
Violations: 0 | |
Latitude: 40.23738771 | |
Longitude: -82.90285767 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1032556554 | 2013-12-18 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Check well, pressures, storage and identification. No change in status from previous inspection.. | Field Visit or Inspection | |||
-1032556554 | 2013-12-18 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Check well, pressures, storage and identification. No change in status from previous inspection.. | Compliance Notice | |||
-1032556554 | 2013-12-18 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Check well, pressures, storage and identification. No change in status from previous inspection.. | Compliance Notice | |||
1053006842 | 2003-05-15 | Well on gravity. | ||||
1057681019 | 2003-07-08 | Injection done on gravity. ID, dikes ok. | ||||
-1074569511 | 2011-05-10 | Check well and storage, Ok. Valves on the well head are closed at this time. | ||||
1078763489 | 2004-03-08 | Plumbing leak at well on elbow has been replaced and repaired.
Well is gravity pressure over 125 on annulus. |
||||
1099057347 | 2004-10-29 | Chk well and storage, Ok. | ||||
1109706002 | 2005-03-01 | Snow cover and snowing. Facility appears ok. Well takes fluid on gravity. | ||||
-1115493886 | 2003-01-30 | Weather: snow covered 25F 9:30 a.m. Inspection w/ Jeff Fry. Integrity of well checked ok. ID was present. Fluid is taken on gravity. | ||||
1187355800 | 2007-08-17 | Chk well and stoage, Storage tank has been removed and the injection line has been unhooked from the well head. The well is incapable of being used for injection at this time. Approx 9:15 AM I talked to Mrs. Harmon and she told me the landowner has her in court over the well and that he is planing on having Jack Fishburne work the well over and set a new tank so that the well can be used. | ||||
1188225343 | 2007-08-27 | On site for MIT. Pressured up to 300 psi, lost 5psi in 15 min, Past test. New tank of the same size has been installed. New well head fittings and injection line installed, quarter inch tap and a new gage on well head. Identification painted on the storage tank. | ||||
1192058254 | 2013-05-07 | Inspect injection well, storage and identification. All valves shut, well shut-in. Currently testing feasibility of placing back online. | ||||
1194011892 | 2007-11-02 | Chk well and storage,Ok. | ||||
1205246539 | 2008-03-11 | Chk well and storage, on my last inspection of 01/18/08 I found that the storage tank needs a lid on the larger opening to prevent some one form falling into the tank. I phoned and told Mrs Harmon ot the problem and requested that a cover be put over the opening. As of this date the lid has not been installed as requested. | ||||
1205766719 | ||||||
1247147848 | 2009-07-09 | Chk well and storage. Valves on well head closed. Vertical tank at storage site has the clean out hatch off of it. | ||||
1255456001 | 2009-10-13 | Chk well and storage, Ok. Valves on tubing closed at the well head. | ||||
1268115589 | 2012-02-29 | Inspect Well. Well shut in. Operator needs to service well and clean out. | ||||
1287i775 | 2002-06-04 | need 1/4 inch valve on tubing . | ||||
1323268510 | 2011-12-07 | An inspection revealed no violations. No injection at time of the inspection. A fitting has been installed on the injection side of well. | ||||
1345641434 | 2012-08-22 | Inspected the Alexander #1 (SWIW #6) as part of a standard quarterly status check. Well is shut-in, back-side annulus pressure 120 psi. The well identification is clearly marked on the storage tank, the well is located inside the dike. Location entry is not marked well and is located at 1426 south galena road. | ||||
1351000233 | 2012-10-21 | Inspected the Alaxander #1 (#160) (SWIW #6) as part of a standard injection well status check. Injection: shut-in, annulus: 125 pounds per square inch. Well identification and site OK. | ||||
1363783062 | 2013-03-20 | Inspect injection well for dike and tank measurements. Dike 36'L x 25'W x 2'D. Tank 21' x 8' horizontal. (188 barrels at 100% capacity). | ||||
1364402602 | 2013-03-26 | Received a forwarded email dated 3/26/2013 from Ms. Betsy Bender 1426 S. Galena Rd. regarding the flow line to the Alexander #1 (#160) (SWIW #6) which had parted. Contacted Ms. Bender 3/26/13 and discussed her concern that the line is broken and it may have caused a leak. Explained to her that the well is not in use and the line is shut-in on both sides (injection well and production well). Inspected the well on 3/26/13 and found the line had separated at a line slice (hose clamp came loose). No release occurred. Called Mr. Harry Kallipolitis of the Ohio EPA and informed him of the findings. Informed Inspector Tom Benko (UIC) of the findings and he met with the operator on location 3/27/13. Status: ok. | ||||
1364563310 | 2013-03-27 | Inspect well, tanks and flow line with Bill Jackson, well tender. An Email message has been received identifying a broken flow line. During the inspection and site meeting it was reported the flow line previously broke due to a fallen tree with an oversized root ball. This break was repaired with a plumbers fitting and hose clamps. This splice was parted during the inspection. Inspection of the line revealed a total of three historic mechanical splices in the valley. No fluids were released from the flow line as the well has not been in production for an extended period of time. A previous repair the line is present near the production tanks, a new section of line was welded in place for this repair and is not of concern to this issue. The well and flow line have been shut in for several years and have not been utilized. During This inspection and previous inspections the operator reported that the well required servicing. The operator shall either repair the line, under the supervision of DNR inspectors, then pressure test the line, and put the well into production. Notification of the inspector is required prior to injecting fluids into the well. Or, remove the line and plug the injection well. The operator is being notified that a resolution is required within 60 days of this inspection report. | ||||
1385130763 | 2013-11-21 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Check well, pressures, storage and identification. Status: well is not in operation. | ||||
1389993309 | 2014-01-17 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Check well, pressures, storage and identification. No change in status from previous inspection. | ||||
1390920086 | 2014-01-28 | Location Information. ENTRANCE: Lat. 40.23727 Long. -82.89856 / WELL HEAD: Lat. 40.23731 Long. -82 .90269 / CENTER-OF-STORAGE: Lat. 40.23729 Long. -82.90266. NOTE: the well head is located inside the storage dike. | ||||
1394803872 | 2014-03-14 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Inspect well, pressures, storage and identification. Status: no change in status from previous inspection. | ||||
1407441478 | 2014-08-08 | Inspect well for integrity and check pressures. Well is shut in. Storage tank is empty. Tank bottom is rusted near the inlet valve. The tank will need to be replaced or repaired prior to injection start up. The Flow line from the production well to the injection storage tank has not been replaced and is shut in. | ||||
1408711772 | 2014-08-22 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Inspect well, pressures, storage and identification. Status: No change in status from previous inspection. | ||||
1414419743 | 2014-10-27 | Provided Reports requested. Compliance Notice satisfied. | ||||
1415129240 | 2014-11-04 | Inspect well for integrity and pressure. Well is shut in. Met with Bill Jackson on location. Storage tank at well head has rusted through along weld at base of tank. The flow line from the production line to the brine storage tank needs to be replaced. | ||||
-14245604 | 2004-02-12 | Met Mrs. Harmon (Pat). Husband Clint, passed away in January.This is the first time she has been to the well since. Small drip leak on injection line at 1 1/2 elbow. Plastic bucket placed under it until repaired. Mrs. Harmon will call when repaired. Did | ||||
1426076701 | 2015-03-10 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Inspect well, pressures, storage and identification. Status: no change in status from previous inspection. | ||||
-1450119292 | 2009-12-16 | Check well and storage, Ok. Vaves on well head are closed. | ||||
147769300 | 2005-10-20 | FAILURE TO SUBMIT ANNUAL SALTWATER INJECTION WELL REPORTS | ||||
1523915151 | 2010-08-02 | check well and storage, Ok. | ||||
-1578036407 | 2008-09-04 | Chk well and storge, Ok. | ||||
-1624504102 | 2014-04-03 | Inspect location with NW Regional Supervisor, William Ziegler. | ||||
-1656724318 | 2006-05-19 | Chk well and storage, Valve on the annulus is leaking and I can not chk the pressure. It has possitive pressure but has not been tested for some time. A pressure tset should be scheduled soon. The tank at the well head is full of holes and should be emptied and removed. | ||||
1686462050 | 2011-06-06 | Accompanied Brent Bear and Josh Garland on inspection. | ||||
1743075808 | 2013-08-21 | Inspected the Alexander #1 (SWIW #6) as part of a standard injection well status check. Check well, storage and identification. The injection well remains out of service. | ||||
1795619021 | 2004-05-26 | GPS updated. No activity at disposal site. | ||||
1831314502 | 2009-02-20 | Chk well and storage, Ok.
Light snow cover. |
||||
1833493327 | 2012-05-21 | Inspect Well. Shut in. | ||||
1843020609 | 2011-09-21 | An inspection revealed no violations at this time. Unable to obtain injection pressure at this time, as there is no fitting available for gauge installation. Notified Mr. Bill Jackson, the representative for Patricia Harman to install 1/4 fitting on injection side. This location was tagged with ribbon for him to also reference. Note: Saltwater line from Permit 129 to this location had released brine and line has since been fused together and cleanup is ongoing. Please refer to Inspect Reports under Permit 129 for more details. | ||||
-1915680927 | 2006-12-14 | Inspected well with Jeff Fry. There was no ID posted at the tank battery or the wellhead. There was no quarter inch tap on the injection, however it was determined that there was 0 psi. It was determined that there was positive pressure on the annulus. | ||||
-1971798664 | 2008-12-12 | Check well and storage, Ok. | ||||
-1977319963 | 2014-05-29 | Inspected the Alexander #1 (SWIW #160) as part of a standard injection well status check. Inspect well, pressures, storage and identification. Status: no change in status from previous inspection. | ||||
1979080600 | 2007-02-06 | There was no ID posted at the tank battery or the wellhead. There was no quarter inch tap on the injection, however it was determined that there was 0 psi. It was determined that there was positive pressure on the annulus. I talked with the pumper Bob Bell. He indicated that the injection well is currently not in production and won't be until the spring when they plan to bring in a new tank. | ||||
2020863809 | 2011-06-06 | An inspection revealed no violations at this time. No injection at time of inspection. | ||||
-2043322253 | 2013-02-28 | Standard injection well status check, well is currently not being used for injection. Site, storage, identification ok. | ||||
-2092321176 | 2006-06-22 | On site for routine inspection. The annulus has not been pressure tested for some time the well head fittings( i.e.: valves) will not allow for monitoring of the pressure due to deteriorated conditions.
A pressure test w/an inspector on the site should be arranged. |
||||
281644619 | 2007-08-22 | Chk. Well and storage, new tank installed and all new fittings. New valves on well head, new injection line and filtration the well needs to have an MIT before starting to inject water. Valves on well and at the tank are closed at this time. Called Mrs Hrmond at approx. 1:50 PM talked about the pressure test and other miner leaks at the production site. | ||||
-460153209 | 2008-01-18 | Chk well and storage, Ok. | ||||
-53895292 | 2006-02-02 | Chk well and storage, need to pressure test the annular space. Storage tank at the well head should not be used, it has holes in the side and is not liquid tight. | ||||
697622056 | 2009-03-19 | Chk well and storage. | ||||
707073089 | 2006-12-01 | Storage tank at the well head has been removed. Injection line unhooked, well not in use. | ||||
757029621 | 2010-03-30 | Chk well and storage, ok. | ||||
-766765191 | 2014-10-07 | Our records indicate that the Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on February 15, 2013. The Disposal Fee report for the 3rd and 4th Quarter of 2013 needs to be filed also. | ||||
783864130 | 2011-06-06 | accompanied B.Bear on status check of SWIW well. |
For data sources see[1]