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34-077-20172

Well Details

Well ID: 34-077-20172
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County: Huron
Municipality:
Operator Name: ORPHAN WELL PROGRAM
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1985-09-20
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 41.10590607
Longitude: -82.48537753

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 1484.0 0.0
1986-0 2830.0 0.0
1987-0 1676.0 0.0
1988-0 76.0 21.0
1989-0 0.0 0.0
1990-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1287900327 2005-11-23 Inspect Well. Pump jack; No motor. No ID. Moderate sour gas odor. Incapable of production. Plug permit has expired.
1305970835 2001-09-18 FOLLOW UP TO NOV # 84 Follow up on NOV # 23011. No change since last inspection by Insp. Mike Phelps. Well refered to orphan program.
-1309839579 2012-04-27 Petroset pump cement through tubing to set bottom plug with 50/50 Poz.
1492553095 2001-09-17 FOLLOW UP TO NOV # 90 Follow up on NOV # 23011. No change since last inspection by Insp. Mike Phelps. Well refered to orphan program.
15832692 2011-05-09 Inspect well. Well with 4.5 inch casing, slips with 1.5 inch tubing, rods pump jack, rusted and leaking.
-1832595104 2012-10-29 Inspect well location. Final restoration is complete and good. Land owner waver has been received to leave the plastic flow lines in the ground. Corn is standing. Measure with GPS the area impacted for crop damage; about 0.6 acres affected.
1885316095 2004-11-09 Crops in field. Direct inspection of well not possible. Inspection from road indicates pump jack is overgrown with vegetation. Id is not visible. Common tank with new id posted for permits 165, 171, and 172. Tank has been emptied.
-1910109812 2012-05-07 Petro set was contacted to reset bottom plug with Class A Cement with loss circulation material including cotton seed hulls and cell flake and 3 % calcium chloride. Plug was bull headed into formation and pressured up to 1200 pounds of pressure.
-1925219945 2012-05-07 Approval was granted by Mike McCormac at 11:58 AM for plugging contractor to bull head well with Class A cement to kill well and set bottom plug second time due to thief of cement. No Hydrogen Sulfide Gas was observed during work.
2030207918 2012-05-04 Contacted by Plugging contractor to report that formation thieved the 50/50 Poz cement and the well blew out when setup to clean out for topping off well.
-2140313118 2008-04-23 Inspect well. Pump jack, no motor. Heavily overgrown with vegetation. 1.5 inch tubing, 4 inch long string. STRONG ODOR FROM WELL.
-4024422 2003-04-04 Inspect Well. 8 slips to 4 pipe, Tee, and slips to 1.5 string. Polish rods. Pump jack. No motor. No Identification. Valves Rusted and closed. Well incapable of production. Moderate Odor of gas.
557483632 2004-12-08 Inspect Well. Plug application has expired. Pump jack on well, shut in. overgrown with vines. No ID posted at well head. New ID is posted at common tank with ID 165 and 171.
-805728942 2012-05-16 Top off well with 9 sac grout to surface. Moritz of Ashland delivered cement.
8473527 2001-09-18 Follow up on NOV # 23011. No change since last inspection by Insp. Mike Phelps
9073533 2001-09-17 Follow up on NOV # 23011. No change since last inspection by Insp. Mike Phelps.
941532434 2004-06-17 Inspect tanks, update tank location. 1 - 100 bbl common tank with permits 171.
CEN3228 1998-12-30 1509.12

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.