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Well ID: 34-157-25391 | Loading map...
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County: Tuscarawas | |
Municipality: | |
Operator Name: L L P OIL & GAS CORP | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2008-08-21 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 40.30568207 | |
Longitude: -81.35829298 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2008-0 | 0.0 | 68.0 | ||||
2009-0 | 2871.0 | 160.0 | ||||
2010-0 | 2931.0 | 83.0 | ||||
2011-0 | 2816.0 | |||||
2012-0 | 1025.0 | 111.0 | ||||
2013-0 | 1509.0 | 46.0 | ||||
2014-0 | 1141.0 | 365.0 | 21.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1397242175 | 2014-04-11 | At 8:30 am I received a call from inspector Berry Grimm on a complaint. It was from an anonymous person that the Vickers Unit had a breech of the dike and Brine was leaking. Upon arriving on location I found 2 - 210 bbl tanks, 1 - 100 bbl, and a 30 bbl plastic tank. All were in an earthen dike, and properly identified. I could not identify any breech in the dike. There was standing water in the dike. A water truck hose was connected to one of the 210 bbl tanks and it was leaking. I obtain a water sample of the water in side the dike, and tested with quantab and found the chlorides to be above 6000 ppm. I contacted Mark Clark with LLP at 11:30 am and advised him of the occurrence and instructed him to disconnect or plug the hose. To remove the water from the dike and dispose of it as being Brine water at a permitted injection well felicity. | ||||
1403011737 | 2014-06-17 | On the day of my inspection I found the dike area to be rebuilt. The east end has been replaced and height add, with clay material. The stressed area is in the process of remediation. Lime and Manure have be applied. | ||||
-446266932 | 2014-04-21 | On the day of my inspection I found Mark Clark and crew from LLP, rebuilding the dike around the tank battery to prevent furather leaching of fluid. | ||||
-642363347 | 2009-10-26 | no violations | ||||
-78346774 | 2009-10-26 | restoration approved |
For data sources see[2]