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34-157-25391

Well Details

Well ID: 34-157-25391
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County: Tuscarawas
Municipality:
Operator Name: L L P OIL & GAS CORP
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2008-08-21
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.30568207
Longitude: -81.35829298

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2008-0 0.0 68.0
2009-0 2871.0 160.0
2010-0 2931.0 83.0
2011-0 2816.0
2012-0 1025.0 111.0
2013-0 1509.0 46.0
2014-0 1141.0 365.0 21.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1397242175 2014-04-11 At 8:30 am I received a call from inspector Berry Grimm on a complaint. It was from an anonymous person that the Vickers Unit had a breech of the dike and Brine was leaking. Upon arriving on location I found 2 - 210 bbl tanks, 1 - 100 bbl, and a 30 bbl plastic tank. All were in an earthen dike, and properly identified. I could not identify any breech in the dike. There was standing water in the dike. A water truck hose was connected to one of the 210 bbl tanks and it was leaking. I obtain a water sample of the water in side the dike, and tested with quantab and found the chlorides to be above 6000 ppm. I contacted Mark Clark with LLP at 11:30 am and advised him of the occurrence and instructed him to disconnect or plug the hose. To remove the water from the dike and dispose of it as being Brine water at a permitted injection well felicity.
1403011737 2014-06-17 On the day of my inspection I found the dike area to be rebuilt. The east end has been replaced and height add, with clay material. The stressed area is in the process of remediation. Lime and Manure have be applied.
-446266932 2014-04-21 On the day of my inspection I found Mark Clark and crew from LLP, rebuilding the dike around the tank battery to prevent furather leaching of fluid.
-642363347 2009-10-26 no violations
-78346774 2009-10-26 restoration approved

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.