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34-129-20107

Well Details

Well ID: 34-129-20107
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County: Pickaway
Municipality:
Operator Name: OHIO ENERGY ASSETS, INC.
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1995-08-03
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.63640749
Longitude: -82.96920658

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1995-0 0.0 4484.0
1996-0 0.0 148.0
1997-0 0.0 0.0
1998-0 0.0 0.0
1999-0 0.0 3433.0
2000-0 0.0 4714.0
2001-0 0.0 2214.0
2002-0 0.0 2072.0
2003-0 0.0 1063.0
2004-0 0.0 695.0
2005-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1031664847 2002-09-10 Inspection revealed NO MOTOR on pumping unit. OWNER NEEDS to place well into production and/or plug said well. If well is placed back into production OWNER NEEDS to place the proper ID at the well. Inspector updated Lat/Long this date. WEATHER CONDITIONS: Sunny and 75 degrees. 09/11/02 I spoke with Joe and advised him of the violation. He advised me he was working on the well and should have it back into operation by 11/10/02. I advised him that will be ok and I will follow-up on or about that date. Compliance Notice
1031664847 2002-09-10 Inspection revealed NO MOTOR on pumping unit. OWNER NEEDS to place well into production and/or plug said well. If well is placed back into production OWNER NEEDS to place the proper ID at the well. Inspector updated Lat/Long this date. WEATHER CONDITIONS: Sunny and 75 degrees. 09/11/02 I spoke with Joe and advised him of the violation. He advised me he was working on the well and should have it back into operation by 11/10/02. I advised him that will be ok and I will follow-up on or about that date. Compliance Notice
1031664847 2002-09-10 Inspection revealed NO MOTOR on pumping unit. OWNER NEEDS to place well into production and/or plug said well. If well is placed back into production OWNER NEEDS to place the proper ID at the well. Inspector updated Lat/Long this date. WEATHER CONDITIONS: Sunny and 75 degrees. 09/11/02 I spoke with Joe and advised him of the violation. He advised me he was working on the well and should have it back into operation by 11/10/02. I advised him that will be ok and I will follow-up on or about that date.
-1117169186 2002-09-10 FOLLOW UP TO NOV # 1031664847 Inspection revealed NO MOTOR on pumping unit. OWNER NEEDS to place well into production and/or plug said well. If well is placed back into production OWNER NEEDS to place the proper ID at the well. Inspector updated Lat/Long this date.
1132238474 2005-11-10 Tubing pulled from well, 4 1/2 casing rip total of 1,416.85 retrieved from well. Formation Cementing and Berry Well Service doing work.

4 Plugs and 3 gel spacer set. Plugging of well will pass NOV.

1248i167 2002-01-18 No violations noted this date.
-1301193119 2004-02-04 - Follow up inspection of NOV issued by inspector Keith White on Sept. 11, 2002

- Noted pump unit working this past summer of 2003. - No motor on well at time of inspection. Will contact operator of intent of this well. - Contact Joe Melville (2/06/2004)

-133124908 2004-10-05 Preliminary inspection was done by previous inspector. Well has ID in place.
-1489708731 2004-10-05 #NAME?
-1812922737 2006-01-10 - Well was plug in Oct. of 2005

- Operator has removed all tubing, and all equipment from well area. Area has been graded, the land is put back to agricultural use.

-701279777 2003-12-03 Operator has motor removed from pump jack, production valve is open.
730085483 2005-01-26 #NAME?
VER1047 1998-04-02

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.