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34-169-25561

Well Details

Well ID: 34-169-25561
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County: Wayne
Municipality:
Operator Name: HARLEY DRILLING & PRODUCI
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2007-03-27
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.88695357
Longitude: -81.98970168

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2007-0 833.0 0.0
2008-0 3156.0 0.0
2009-0 2352.0 175.0
2010-0 3051.0 0.0
2011-0 949.0 0.0
2012-0 873.0 0.0
2013-0 1208.0 332.0
2014-0 675.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1279606408 2007-03-27 Check on Capstar Drilling and found rig at 463 ft. on 11 surface hole .One pit lined and the other pit is open , no fliud or liner .
1457518139 2012-11-29 This is a producing pump jack well. There were no problems noted at the time of the inspection.
1580680368 2007-04-05 Plug well back to the Clinton .Petroset and Capstar Drilling .
1738920473 2007-03-28 Arrive for Cement on casing and while running 8 inch in well the casing parted at the threads on the last joint .Now it needs to be fished out and tested .Casing fell 100 ft.
1805414322 2007-04-16 Check on Clinton plug back and found that 4 inch remains and pits are full, liner in place .
-1815072817 2008-03-24 Meets requirements for Primary Restoration.
2091928466 2013-09-30 This pumping unit well has no apparent problems at time of inspection.
-2130287005 2014-12-16 This is a pumping unit well that has no apparent problems at time of inspection.
76620594 2007-04-04 Capstar Drilling at 5165 ft on 7 7/8 hole soaping .All safety equipment in place ,blow line chained and staked ,manifold connected .
952977903 2007-03-29 Capstar Drilling fished out 8 inch casing and ran new string in to 929 ft and c/w 300 sks - Petroset John

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.