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34-129-20202

Well Details

Well ID: 34-129-20202
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County: Pickaway
Municipality:
Operator Name: HOUGHTON INVESTMENTS, L.L.C.
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2004-04-06
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.61033788
Longitude: -83.06336284

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2004-0 0.0 830.0
2005-0 0.0 958.0
2006-0 0.0 517.0
2007-0 0.0 428.0
2008-0 0.0 214.0
2009-0 0.0 209.0
2010-0 0.0 285.0
2011-0 0.0 134.0
2012-0 0.0 188.0
2013-0 0.0 185.0
2014-0 0.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1107189784 2005-01-26 - Well not operating while on site, notice oil leaking to surface from production pipe between pump unit and tank battery. Notify Tom Atha and shut power off to pump unit area of oil is about 10ft X 20ft.

- Water reading from meter 305330 gals = 7269 barr

Phone Call
1118237701 2005-06-07 - Pump unit operating while on site, ID on tanks, area clean.

- Water meter reading 305877 gallons = 7282 barrels 13 barrels since last reading in April 2005.

-1157739821 2006-03-08 - Pump unit not operating while on site. ID on tank.

- Well and tank area clean and well maintained, area between well and tanks has had topsoil removed, this area is where production line broke last year. - Water meter not working, has same reading that

1353147595 2009-06-10 #NAME?
1366181508 2005-02-02 Follow up inspection to NOV issued 1/26/2005. Operator has lay temporary production line from pump unit to tanks, operator has removed soil that was saturated with oil.
1377184369 2013-08-22 - Pump unit not operating while on site. ID on Tank.
 1- 210 steel tank and 1-100 steel tank
Area clean and free of debris.
1402927455 2014-06-16 - On site for plugging well, tubing and rods has been removed prior to arriving on site today.

- Berry Well Service doing service work, Formation Cementing Co. cement contactor. - 1st plug set at 2430 to 2130 - 4

-1441016795 2008-09-10 #NAME?
-1710793945 2004-10-06 well not operating while on site, area around well and tank clean and free of water.

Water meter reading 294298 gal = 7007 barrels

178733289 2004-07-29 Joint inspection with Jeff Fry.

- Operator has well in production, 2 - 210 barrel tanks and 1 - 100 barrel water tank. - Operator is pumping water to McCloud # 1 for disposal. Water meter reading 200749

1836097590 2008-06-11 #NAME?
-1965846471 2011-04-21 #NAME?
1987175469 2009-01-06 - Pump Jack not operating while on site. ID on Tank. Dike area free of water.

- Weather light freezing rain, Temp high 20's

-2098154115 2005-10-04 - Pump unit not operating while on site.

- Water meter reading 306977 gallons = 7,308 barrels

318950419 2006-01-10 - Pump unit not operating while on site, ID on tanks.

- Water meter reading 307348 gallons = 7317 barrels - Weather Cloudy temp 30's

-474837620 2009-04-01 - ID on tank, pump jack not operating while on site.

- Notice that production line has been repaired, band clamp around pipeline. Operator is in the process of cleaning and removing soil.

-825888289 2005-04-05 Pump unit operating while on site, tank area clean and ID in place.

Water meter reading 305330 gal. = 7269 barrels.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.