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Well ID: 34-075-24714 | Loading map...
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County: Holmes | |
Municipality: | |
Operator Name: ATLAS NOBLE LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1987-05-21 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Plugged and Abandoned | |
Violations: 0 | |
Latitude: 40.5737079 | |
Longitude: -81.67048086 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1987-0 | 10806.0 | 0.0 | ||||
1988-0 | 23297.0 | 75.0 | ||||
1989-0 | 16142.0 | 0.0 | ||||
1990-0 | 9159.0 | 53.0 | ||||
1991-0 | 8543.0 | 0.0 | ||||
1992-0 | 6482.0 | 0.0 | ||||
1993-0 | 4216.0 | 0.0 | ||||
1994-0 | 4026.0 | 0.0 | ||||
1995-0 | 2316.0 | 0.0 | ||||
1996-0 | 3056.0 | 0.0 | ||||
1997-0 | 960.0 | |||||
1998-0 | 2867.0 | 0.0 | ||||
1999-0 | 2183.0 | 21.0 | ||||
2000-0 | 2506.0 | 0.0 | ||||
2001-0 | 2331.0 | 0.0 | ||||
2002-0 | 813.0 | 0.0 | ||||
2003-0 | 221.0 | 0.0 | ||||
2004-0 | 278.0 | 0.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2006-0 | 0.0 | 0.0 | ||||
2007-0 | 0.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 0.0 | 0.0 | ||||
2011-0 | 0.0 | 0.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 0.0 | ||||
2014-0 | 0.0 | 130.0 | 0.0 | 130.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
11832 | PASSED Y WITNESSED 9/15/87 INSPECTOR DATE 09/1519/87 DATA FROM OLD VAX INFO | |||||
1385728771 | 2013-11-27 | This well is shut-in. The tank battery has been removed. There is an active Compliance Notice on this well. A plugging permit has been issued for this well. | ||||
1423533063 | 2014-11-05 | Nicks Well Plugging pumped a 30 sack bottom cement plug thru the tubing. Pulled the tubing. | ||||
1754097914 | 2012-03-02 | Well is shut in. Well shall be plugged or put into TI status. Failure to comply with this notice may result in forfeiture of bond. Plugging permit in hand | ||||
-1844749521 | 2014-11-17 | This well has been plugged and abandoned. The compliance notices are satisfied. | ||||
-2131024499 | 2014-11-06 | Tested the casing to 600 psig and it held. Will plug thru the casing. Tried to rip the casing but there was no telegraph until 650'. Called out the perforators and perforated 10 shots from 2808-2798'. Ran tubing and spotted a 200' plug from 2814 to 2614. Pulled the tubing. | ||||
290017808 | 2011-04-27 | Shut in. No production reported since 2004. Plug or produce or place into temporary inactive status. Failure to comply with this notice may result in forfeiture of bond. | ||||
607115382 | 2014-11-07 | Shot 4-1/2' casing off at 1100'. Pulled one joint and tried to break circulation. After 32 bbls was pumped, the pressure went to 500 psig and the casing started coming out of the hole. Released the pressure and tried again and again and finally had to break off the hose and reciprocate the pipe. Hooked up and started pumping and reciprocating the pipe again and finally got circulation after ~ 20 bbls. Circulated for 15 minutes and spotted the Berea/Casing plug from 1056 to 856'. Pulled 21 joints ans spotted the top plug. The plug stayed up. See the plugging report for more details. | ||||
PL15124 | Preliminary Restoration done information from Data Point |
For data sources see[2]