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34-089-26128

Well Details

Well ID: 34-089-26128
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County: Licking
Municipality:
Operator Name: KNOX ENERGY INC.
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-05-28
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.10085896
Longitude: -82.64608507

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 0.0 210.0
2014-0 0.0 365.0 532.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1278379918 2013-05-30 I witnessed the cementing of the 8 inch surface casing for Knox Energy on Kilbarger rig 5. Bill Mitton with Knox Energy was on location. Petroset Cementing was contracted to cement the casing. Circulation was established. Partial cement returns were observed. A cement basket was not installed.
1372869555 2013-05-31 I inspected drilling operations today. Kilbarger rig #5 drilling on air with 7.88 bit. Depth approximately 1,680 feet during inspection. No violations this date.
-1435228971 2013-07-16 This inspection was conducted as a preliminary restoration status check. The well was equipped with a pumping unit and motor. The pits used during drilling have not been closed. Knox Energy will be closing the pits this week .
-1599051356 2013-05-29 I inspected drilling operations today. Kilbarger rig 5 drilling on fluid during inspection. Depth was approximately 287 feet. No violations this date.
573694346 2013-06-07 Bill Mitton with Knox Energy called to inform me that the backside of the 8 surface casing had caved in approximately 15 feet down. He was called in a cement mixer to grout the backside of the casing from the surface with 9 sack grout. I witnessed this job and cement stayed at the surface.
-731355902 2013-06-14 I witnessed this frac job for Knox Energy. Producers Service Corp. was contracted to frac this well. Refer to stimulation report for details.
-78471032 2013-11-25 This inspection was conducted as a preliminary restoration status check. The well was equipped with a pumping unit and motor. A GPS reading was taken at the wellhead. The well is located in an agricultural field. The area around the well has been restored. The tank battery consists of (1) 210 barrel tank and (2) 100 barrel tanks inside an earthen dike. A GPS reading was taken at the tank battery location. This well shares the tank battery with p# 3646. Identification posted at wellhead and tank battery. Inspection meets ORC 1509.072 requirements. Weather: 22 degrees F, Clear
790746894 2013-07-16 I inspected this well location today. The well was equipped with a pumping unit and motor. The well was pumping during inspection. The drilling pits were open. Knox Energy will be closing the pits this week.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.