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34-067-20317

Well Details

Well ID: 34-067-20317
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County: Harrison
Municipality:
Operator Name: SOUND ENERGY CO INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1976-12-08
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.42635467
Longitude: -81.22083223

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1986-0 1119.0 630.0
1987-0 1072.0 83.0
1988-0 1771.0 0.0
1990-0 531.0 0.0
1991-0 361.0 0.0
1992-0 319.0 0.0
1993-0 435.0 0.0
1994-0 255.0 0.0
1995-0 0.0 0.0
1996-0 0.0 0.0
1997-0 15.0 0.0
1998-0 198.0 0.0
1999-0 157.0 0.0
2000-0 90.0 0.0
2001-0 177.0 0.0
2002-0 115.0 0.0
2003-0 101.0 0.0
2004-0 273.0 0.0
2005-0 33.0 0.0
2007-0 1.0 0.0
2008-0 15.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1340833118 2012-06-25 The well is idle. The last reported production was in 2008 for 15 thousand cubic feet (MCF) of gas. The well is not legibly identified. The well operation has pollution inside and outside the well head dike. The tank battery was not located. According to land owner, Ken Fouts, the tank battery has been removed. Plug, produce or sell this well. Clean up contaminated soil and dispose of it at a facility approved for solid waste. Legibly identify well. Failure to comply with this request may result in forfeiture of bond.
1344948962 2012-08-13 I am on site to respond to a call from OEPA that was called in this afternoon. I found that there is a 28 ft. x 12 ft x 2 ft dike around a non producing well. The dike has 8 to 15 gallons of crude oil and brine inside the contained area. I contacted Bruce Levengood @ 330-364-7665 and advised of the on going contamination at his well location. He said he would call for a water truck and other equipment to remove the oil and contaminated soil in the dike and around the well. He said he felt he could be on site Tueday 08/14/2012 or Weds at the latest. He is to contact me when he is going to be conducting the clean up activity so I can be on site.
1367418677 2012-11-20 I am on site today to witness the plugging of this well. Berry Well Service has a service rig on location and Omegea Cementing is on site to pump cement. The well has 2 3/8 inch diameter tubing in it. The tubing has parted and could not be fished out. So it was determined that the 4 1/2 inch casing would be loaded with freshwater and if it went on vacuum a plug could be sent to the bottom even though tubing is in the hole. A string of 2 3/8 inch tubing was installed to 1469 ft. Omega mixed 100 sks of Class A cement and displaced it to that depth. The well was packed off and the 4 1/2 inch diameter casing was pumped up and Omega displaced 54 bbl of water to place the cement to the perfs. Then the tubing was pulled and the casing ripped at 1469 ft. tubing was run back in the well and a plug was set from 1163 ft to 1463 ft. The last plug was from 200 ft to surface. Cement was circulated to surface where it remained after the job was complete.
-225078165 2013-04-30 I am checking today to see if the final restoration can be passed. I found that the equipment used to produce the well has been removed and the area graded but not seeded. Contacted Bruce Levengood and advised that the site will need further grading and seeding before the final restoration can be passed.
22776054 2002-04-23 Road blocked either by owner or operator? Could not access wellsite.
23876063 2002-04-23 Access road is blocked ? Check tanks only.
-280269428 2013-07-25 Everything passed according to 1509.072B.
-517111214 2012-11-27 This well has been plugged to surface and I am checking to see if there are any leaks. I did not find any leaks but I did find that the 8 5/8 inch diameter surface casing needs to be cut off 36 inches below ground level and the remaining equipment removed. Contact Sound Energy and advise them that the casing can be cut off.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.