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Well ID: 34-013-20898 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
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Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2015-05-01 | |
Unconventional: | |
Configuration: | |
Well Status: Drilling | |
Violations: 0 | |
Latitude: 39.88017699 | |
Longitude: -80.98378424 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1430397152 | 2015-04-30 | Patterson 238 has mobilized to this pad and intends to spud today. No violations noted. | ||||
-1636583722 | 2015-05-01 | On the date of inspection I am on site to witness the cementing of the surface casing. I was informed by Gulfport consultant, Josh Elliot, that the Patterson 538 rig had drilled a 24 inch diameter hole to a depth of 358 feet. Wyoming Casing Services set 18.625 inch, 87.5lbs/ft casing on bottom. I field titrated chlorides with a Quantab and found the level to be 32ppm. Stingray pumped 541sk of Class H cement, 15.6ppg, 1.21 yield, 3% CaCl2, 0.15% CL-HV, 0.15% C-41P. Stingray displaced cement with 97bbl of fresh water. Plug was bumped, floats held, and 19bbl of cement returned to surface. | ||||
-251914706 | 2015-05-15 | Operator failed to get cement returns back to surface during the 9.625 cement job. A temperature log was ran and it was determined that a cement bond log would be required to determine the top of cement. Remedial action will be decided following the bond log. | ||||
6307862 | 2015-03-12 | On this day the 26 casing was cemented in a 30 open hole to a depth of 110'. Stingray ran 256 sks of class A cement with cement to surface established. See cement ticket for details. No violations noted. |
For data sources see[1]