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34-133-22310

Well Details

Well ID: 34-133-22310
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County: Portage
Municipality:
Operator Name: WHITE ENERGY INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-03-03
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 41.23438392
Longitude: -81.1423594

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 2740.0 1575.0
1985-0 2378.0 1041.0
1986-0 941.0 338.0
1987-0 812.0 608.0
1988-0 452.0 484.0
1989-0 771.0 1030.0
1990-0 618.0 936.0
1991-0 703.0 665.0
1993-0 460.0 570.0
1994-0 339.0 555.0
1995-0 256.0 397.0
1996-0 237.0 487.0
1997-0 235.0 456.0
1998-0 0.0 248.0
1999-0 59.0 0.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 0.0
2005-0 0.0 0.0
2006-0 0.0 0.0
2007-0 0.0 0.0
2009-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1004707594 2011-05-04 I preformed a status check on the plugging of this well. Nick's Well Plugging is preforming the plugging of this well. There were no violations at this time. Compliance Notice
1004707594 2011-05-04 I preformed a status check on the plugging of this well. Nick's Well Plugging is preforming the plugging of this well. There were no violations at this time. Compliance Notice
1004707594 2011-05-04 I preformed a status check on the plugging of this well. Nick's Well Plugging is preforming the plugging of this well. There were no violations at this time. Phone Call
1019208596 2002-01-23 FOLLOW UP TO NOV # 1216i185 01-23-2002 Well remains shut in. The company was going to sell this well, but has failed to do so for two years now.
1043474776 2011-05-03 Nick's Well Plugging is on site to start plugging and abandoning this well. The first step will be to run an impression block to determine the condition of the downhole rods and tubing which will need to be recovered before plugging.
1216i185 2002-01-23 01-23-2002 Well remains shut in. The company was going to sell this well, but has failed to do so for two years now.
1258061719 2009-10-27 I received a call from the landowner requesting a site inspection and a status update for this well. White Energy has removed the pump jack and a majority of the tank battery. According to Dallas White, he would like to place the well back in production but both tubing and rods are lost in the hole and stuck. He is meeting with his parterns to discuss the well.
1299766566 2011-03-10 Repeated requests to White Energy over the last 18 months, to either plug or produce this well have been unsuccessful. The well must now be properly plugged and abandoned within the allotted time. Failure to comply will result in a material and substantial violation being issued with bond revocation and an cease operations order. Please contact me as soon as a plugging contractor is scheduled.
1305485866 2011-05-11 Fished for more rods. Recovered a total of 137 joints of rods. Ran into hole with 2 3/8 tubing and overshot. Ready to cement tomorrow. There were no violations at this time.
1462759628 2011-08-30 The vegetation is growing on the location. The tank battery, debris is gone. This well PASSES FINAL RESTORATION.
-1968364415 2011-05-18 The fence around the tank battery has been taken down and hauled off the location. The pit is closed. There were no violations at this time.
287704087 2011-05-03 I met with Bob Worstall at the site. Nick's Plugging rig will perform the plugging on this well. The workover rig rigged up. It was raining. The rig pulled 12,000# on the tubing. Will start tomorrow on trying to pull the tubing out of the well. There were no violations at this time.
293969379 2011-05-10 I witnessed the pulling of the 450' of 5/8 rods. The rod overshot broke as well as the rod elevators. Will replace and be back tomorrow. There were no violations at this time.
-456671901 2011-05-12 Cemented the Big Lime, Berea and the surface with Nick's Well Service. There were no violations at this time.
-622668223 2011-03-10 FOLLOW UP TO NOV # 1299766566 Repeated requests to White Energy over the last 18 months, to either plug or produce this well have been unsuccessful. The well must now be properly plugged and abandoned within the allotted time. Failure to comply will result in a material and substantial violation being issued with bond revocation and an cease operations order. Please contact me as soon as a plugging contractor is scheduled.
905506764 2011-04-12 This status check inspection found that the wellhead is not leaking nor is there evidence of past problems. Historical issues would be noted by stained soils and/or stressed vegetation. White Energy has applied for a plugging permit which should be issued within 10 days. Nick's Well Plugging has been contracted to perform this service as soon as it can be scheduled.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.