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Well ID: 34-121-24418 | Loading map...
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County: Noble | |
Municipality: | |
Operator Name: CNX GAS COMPANY LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2013-05-18 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 39.83777514 | |
Longitude: -81.39305596 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2014-3 | 9451.0 | 4.0 | 1375.0 | 4.0 | ||
2014-4 | 97612.0 | 30.0 | 6240.0 | 30.0 | ||
2015-1 | 196932.0 | 60.0 | 7569.0 | 60.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1102375915 | 2013-07-01 | My inspection today finds the drilling rig (Savanna 640) is making up their bottom hole assembly and preparing to drill the 17.5 section of the well. | ||||
1239415253 | 2013-07-08 | The drilling rig is currently hooking up equipment to pressure test the 13.375 casing string. | ||||
-1272997038 | 2013-07-22 | My inspection today finds the rig crew is running 7150' of 9.625 casing. | ||||
1370167318 | 2013-06-01 | My inspection today finds the drilling contractor Eviro-spud is ran 309' of 20 casing. Calfrac cemented the casing in place with class A cement. 20 bbl of cement returns to surface. | ||||
1374776608 | 2013-07-17 | My inspection today finds the drilling rig has shut down due to the top drive being broken. Current depth is 5088'. | ||||
1375297606 | 2013-07-25 | I received a call from CNX stating that they had a diesel spill on location. Upon my arrival the spill was 95% cleaned. The estimated total of the spill was 56 gallons with 50 gallons being held on the primary containment. All material off of containment that was impacted was hauled off to a disposal facility. | ||||
1417801255 | 2013-07-23 | I am onsite to witness the second stage cementing of the 9.625 casing The stage tool is set at 4262'. Calfrac circulated 882 sks of 13.8# cement into place. I witnessed 30 bbl of cement returns to surface. | ||||
-1596835850 | 2014-11-06 | My inspection today finds the site meets the preliminary restoration requirements. The tank battery is comprised of eight 500 barrel tanks set in a metal dike with a plastic liner. Four 500 barrel temporary tanks are set on site in a plastic liner. A liquids pump system is set up at the back of the production site along with a large compressor. Vegetation has been established around the site. | ||||
-1665470305 | 2013-07-12 | My inspection today finds the operator is drilling the 12.25 section of the well at a depth of 2433' | ||||
277319173 | 2013-06-08 | Redstone drilling ran casing to a depth of 313'. Calfrac circulated 629 sks of class a cement. There were no cement returns to surface. Weatherford will bond log the well to find cement top. | ||||
-417719886 | 2013-05-30 | My inspection today finds Enviro-spud has drilled to a depth of 249'. The rig is currently broke down. | ||||
-912656021 | 2013-07-23 | I am onsite to witness the cementing of the first stage of the 9.625 casing. Calfrac circulated 978 sks of 15.5# cement into place. | ||||
-997704215 | 2014-11-06 | My inspection today finds the site meets the preliminary restoration requirements. The tank battery is comprised of eight 500 barrel tanks set in a metal dike with a plastic liner. Four 500 barrel temporary tanks are set on site in a plastic liner. A liquids pump system is set up at the back of the production site along with a large compressor. Vegetation has been established around the site. |
For data sources see[2]