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34-055-21594

Well Details

Well ID: 34-055-21594
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County: Geauga
Municipality:
Operator Name: P & S ENERGY INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1989-05-17
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.37249914
Longitude: -81.13057261

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1989-0 5301.0 1938.0
1990-0 6109.0 1925.0
1991-0 4235.0 1433.0
1992-0 2330.0 945.0
1993-0 2096.0 908.0
1994-0 2888.0 1363.0
1995-0 3081.0 834.0
1996-0 2159.0 995.0
1997-0 1857.0 819.0
1998-0 2640.0 992.0
1999-0 2491.0 805.0
2000-0 2297.0 617.0
2001-0 1767.0 769.0
2003-0 2799.0 638.0
2005-0 1459.0 727.0
2006-0 2094.0 809.0
2007-0 1852.0 555.0
2008-0 2044.0 475.0
2009-0 2084.0 656.0
2010-0 1877.0 642.0
2011-0 1844.0 670.0
2012-0 1804.0 517.0
2013-0 1712.0 547.0
2014-0 1240.0 365.0 321.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1367513124 2013-05-02 My inspection found the well to be equipped with a pump jack. The annulus valve was closed. Oil was leaking from the stuffing box and was running across the location. I met with the pumper for P&S and he was in the process of cleaning up the location with absorbent mats and peat sorb. He is going to have a dike built around the wellhead to prevent any further instances. The tank battery consists of two 210 BBL production tanks, a 50 BBL brine tank, and two mechanical separators. The proper identification is located on the tank battery. The lease road is in stable condition. The tank battery and lease road is being shared with permit number 2-1800.
1368618903 2013-05-15 My inspection found the soil that was saturated with oil had been removed. A dike was also constructed around the wellhead. Nothing else has changed since my last inspection.
-251838735 2014-10-23 My inspection found no changes since my last inspection. No violations found.
559135880 2004-01-21 2-210 bbls,seperator,dike , well rabbit

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.