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34-059-23706

Well Details

Well ID: 34-059-23706
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County: Guernsey
Municipality:
Operator Name: KENOIL
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1987-07-16
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.8503076
Longitude: -81.59624259

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1987-0 3298.0 0.0
1988-0 5920.0 6082.0
1989-0 3952.0 1777.0
1990-0 2130.0 844.0
1991-0 2170.0 556.0
1992-0 3553.0 872.0
1993-0 2486.0 476.0
1994-0 1952.0 668.0
1995-0 1842.0 483.0
1996-0 1193.0 501.0
1997-0 859.0 316.0
1998-0 1133.0 503.0
1999-0 1339.0 300.0
2000-0 967.0 350.0
2001-0 1328.0 343.0
2002-0 863.0 348.0
2003-0 56.0 511.0
2004-0 0.0 171.0
2005-0 0.0 0.0
2006-0 0.0 137.0
2007-0 0.0 557.0
2008-0 0.0 412.0
2009-0 0.0 316.0
2010-0 0.0 264.0
2011-0 0.0 300.0
2012-0 0.0 290.0
2013-0 0.0 231.0
2014-0 0.0 365.0 219.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
11380522 2002-09-11 COMPLAINT OF STRONG SMELL OF H2S GAS AT RESIDENCE APPROXIMATELY 1000' SOUTHWEST OF MOBILE HOME. WELL WAS NOT IN CYCLE AT TIME OF INSPECTION, NO H2S NOTED ON METER. TOLD COMPLAINTAINTS IF THEY ENCOUNTERED SMELL AGGAIN TO NOTIFY. WILL NOTIFY COMPANY TO INJE
1194394610 2007-11-04 GUERNSEY COUNTY SHERIFF'S OFFICE CONTACTED ME TO INFORM OF WELLHEAD LEAK ON THIS WELL. THIS WELL HAS A HISTORY OF STRONG HYDROGEN SULFIDE CONTENT. OPERATOR HAS HAD A FLARE CONSTRUCTED TO FLARE GAS OFF. FLARE EVIDENTLY HAD GONE DEAD AND WAS ALLOWING GAS TO ESCAPE INTO ATMOSPHERE. H2S LEVELS WERE AT 200PPM+. PUMPER CONTACTED AND WELLHEAD WAS SHUT IN UNTIL FLARE LINE CAN BE REPAIRED.
-1339014758 2010-04-23 Inspection revealed that well is equipped with pumping unit and tubing and rods and 4.5 production casing and 8 surface casing and 2-100 bbl tanks with dike in place.
1659170277 2008-03-26 SEPERATOR AREA REMEDIATED SINCE LAST INSPECTION.
-1955105258 2006-08-22 PRODUCING WELL.
396661531 2004-09-14 STATUS CHECK, PUMPING UNIT, STRONG H2S IN WELL.
62615716 2005-10-03 STATUS CHECK
9759 PASSED Y WITNESSED 1/7/92 INSPECTOR MIKE PHELPS DATE 01/0719/92 DATA FROM OLD VAX INFO
9760 PASSED Y WITNESSED 6/13/89 INSPECTOR DATE 06/1319/89 DATA FROM OLD VAX INFO

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.