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34-133-20103

Well Details

Well ID: 34-133-20103
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County: Portage
Municipality:
Operator Name: BUCKEYE OIL PRODUCING CO
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1961-12-20
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.01643199
Longitude: -81.0822219

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 4712.0 539.0
1985-0 5586.0 633.0
1986-0 5496.0 667.0
1987-0 4153.0 479.0
1988-0 3196.0 520.0
1989-0 4116.0 540.0
1990-0 3753.0 527.0
1991-0 0.0 550.0
1992-0 3304.0 561.0
1993-0 6617.0 515.0
1994-0 5415.0 471.0
1995-0 4848.0 499.0
1996-0 5088.0 363.0
1997-0 5021.0 382.0
1998-0 4049.0 252.0
1999-0 4172.0 467.0
2000-0 4270.0 424.0
2001-0 4779.0 238.0
2002-0 4628.0 355.0
2003-0 3523.0 232.0
2004-0 3946.0 124.0
2005-0 3831.0 336.0
2006-0 3143.0 207.0
2007-0 3314.0 229.0
2008-0 4831.0 152.0
2009-0 4420.0 116.0
2010-0 5324.0 220.0
2011-0 5218.0 299.0
2012-0 5036.0 274.0
2013-0 4594.0 115.0
2014-0 4587.0 365.0 212.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1817985662 2006-02-01 CASE 05-029 Columbus received a call from Mr. Al Gibble (386-235-4843) reporting possible pollution and gas venting concerns. The complaint was received in November 2005. Several attempts to enter the property were unsuccessful. The property was used for a fireworks manufacturing, storage and sales outlet. The property is fenced in with razor wire. There is some surface spillage at the tank battery but is contained inside the dike. The spill appears to be from years of use rather than a single event. I also detected a slight gas odor but could not identify a specific source. According to Buckeye, the well has been shut in since the end of October because of a dispute with the landowner. They intend on placing the well back in production as soon as the dispute is settled. No violations at this time.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.