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34-105-23739

Well Details

Well ID: 34-105-23739
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-12-04
Unconventional:
Configuration:
Well Status: Well Drilled
Violations: 0
Latitude: 39.12598617
Longitude: -81.92517046

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1001120923 2014-12-09 Witnessed 762 feet of new 20 lb/ft steel casing set in 780 feet of 8 3/4 borehole with 174 sacks of Class A cement, 600 lb gel, and 200 lb CaCl- accelerator. Centralizers placed on the 1st, 8th, and 22nd joint. A basket was ran at the 14th joint. Circulation established and good returns were seen at the surface.
-1264425986 2014-11-26 Reviewed site construction and drilling program with Jeff Burke.
1280995648 2014-12-10 Administered annular disposal fresh water test. 490 psi was held on the 7 intermediate string for the required 15 minutes with only 5 lbs of pressure lost over the testing period. The intermediate string casing pressure was also administered at this time and only 10 psi was lost over that 30 minute testing period. Each test passed.
1397791383 2014-12-08 Bond log ran on backside of 9 5/8 casing and the top of cement noted at 100 feet.
1417746157 2014-12-04 Witnessed 298 feet of new 9 steel casing set in 330 feet of 12 borehole with 150 sacks of Class A cement. Circulation established but no cement returns seen at surface, fluid level dropped out of site after pump truck shut down.
1418199664 2014-12-03 Building site and digging pit.
1418315749 2014-12-09 Witnessed surface casing pressure test. The casing held the required minimum pressure for the testing period. 370 psi was placed on the casing and after 30 minutes it had dropped to 340 psi.
-1746981622 2015-02-25 I was on location with Inspector Josh Garland. The well is currently shut in and there are two pits adjacent to the wellhead.
221269914 2014-12-08 100 feet of 3/4 flex hose was ran between the surface casing and the conductor. Circulation established and good returns seen at surface. Casing pressure test will be administered after cement has been allowed to set up over night.
243319883 2014-12-05 Fluid level checked between surface casing and conductor, noted to be roughly 60 feet down.
86805042 2015-05-14 Checking pit closure for two month restoration requirements. Pits closed but area has not been graded or reseeded yet.
-91917247 2015-02-24 The pits are open and the site has not been graded.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.